bluepeter1994.avi
2:23
15 жыл бұрын
twatti the nutsy game
2:11
16 жыл бұрын
Пікірлер
@gregkiteos1936
@gregkiteos1936 19 күн бұрын
Wow, 30 years ago today.
@ardalhall2767
@ardalhall2767 Ай бұрын
Not long just started working again after 22 years after the boiler certificate ran out on 2002
@Feesh-k2c
@Feesh-k2c 2 ай бұрын
Did they blow the whistles for help causec i think i heard about that but idk
@gballs3223
@gballs3223 3 ай бұрын
And after all this time and that horrible slip blue peter is back and running well at crewe
@Union_Pacific_4014_BIGBOY
@Union_Pacific_4014_BIGBOY 4 ай бұрын
If people say that blue Peter went faster doing it rail tour accident it might be true, but that thing was going like five.
@Bulleidpacific34105
@Bulleidpacific34105 7 ай бұрын
That sounded truly horrifying.
@Joke.ExeTheJokingLookingDevil
@Joke.ExeTheJokingLookingDevil 7 ай бұрын
". Avi" Hmm...How.. *FAMILIAR* ..
@jarofdirt91
@jarofdirt91 Жыл бұрын
you can hear her crying at the end of the video, around 2:09
@bennickss
@bennickss 2 жыл бұрын
what happened to it? where is it now and is it under restoration?
@xjxnebxg
@xjxnebxg Жыл бұрын
yes it’s with new owner and it’s under overhaul and it’s expected to return this year and i can sent the link
@TheLazyFusspot_3428
@TheLazyFusspot_3428 5 ай бұрын
​@@xjxnebxg It's back on the mainline!
@RITCHMO
@RITCHMO 2 жыл бұрын
Was there a diesel pulling at the front?
@xjxnebxg
@xjxnebxg Жыл бұрын
no
@bartholomew_41
@bartholomew_41 2 жыл бұрын
1st Like After 14 Years
@steamgent4592
@steamgent4592 3 жыл бұрын
I'm sure that driver was ticked off the list of experienced steam drivers after he did that !!🤣🤣🤣🤣"no more steam driving for you old chap remember BP?!??!????"😬😬😬😬😒😒😒😒😒😒😒😒
@thebrummierailenthusiasts5329
@thebrummierailenthusiasts5329 3 жыл бұрын
That loco is now in tornadoes livery the apple green livery and British railways on the tender and that loco will surely be coming back into steam soon
@xjxnebxg
@xjxnebxg Жыл бұрын
it’ll be back in steam later this year
@thebrummierailenthusiasts5329
@thebrummierailenthusiasts5329 Жыл бұрын
@@xjxnebxgyes and I’m hoping that it will not have a wheelslip incident like it happened 29 years ago
@xjxnebxg
@xjxnebxg Жыл бұрын
@@thebrummierailenthusiasts5329 I HOPE NOT plus they’ll have the experienced crews this time 💀 it took about over a year to fix the damage after that wheelslip and plus Blue Peter reached 140 mph by wheelslip but that never counts anyways
@thebrummierailenthusiasts5329
@thebrummierailenthusiasts5329 9 ай бұрын
@@xjxnebxgyeah
@thebrummierailenthusiasts5329
@thebrummierailenthusiasts5329 8 ай бұрын
@@xjxnebxgindeed
@BornotB-xi6kg
@BornotB-xi6kg 3 жыл бұрын
that wheelspin sounds like a banshee
@xX_capybara_Xx
@xX_capybara_Xx 3 жыл бұрын
1:43
@eddielovett2455
@eddielovett2455 3 жыл бұрын
SRPS RAILTOUR. I WAS a steward ON THE BUFFET COACH and all Stewards were involved helping with the evacuation of passengers back to the station.. There were many parts and bits of the loco picked up and brought back to the crews coach. Huge damage to the track that all had to be replaced before any other trains were allowed through !!
@vinniecross1092
@vinniecross1092 3 жыл бұрын
I have the Bachmann 00 version even in 1/76 scale and lightly loaded its prone to wheelspin =/
@keithgarr5534
@keithgarr5534 4 жыл бұрын
In the days of steam they used a banker on southbound stopping services to help with the gradient.
@mick35w
@mick35w 4 жыл бұрын
I was at Durham station that night, il never forget the roar across the city as she slipped,
@theq4602
@theq4602 3 жыл бұрын
Do you know how badly the poor old boy driving her was hurt?
@mick35w
@mick35w 3 жыл бұрын
@@theq4602 broken arms supposedly
@harrymurray2515
@harrymurray2515 4 жыл бұрын
Info on this railtour: www.sixbellsjunction.co.uk/90s/941001sr.htm
@mop714
@mop714 4 жыл бұрын
Was at Doncaster 1970 when they renamed her Blue Peter. My father was a fitter engineer for LNER, British Rail, and serviced the Flying Scotsman, Mallard etc.
@paulcaswell2813
@paulcaswell2813 4 жыл бұрын
Blue Peter from building in the late '40s. The loco was never renamed.
@mop714
@mop714 4 жыл бұрын
@@paulcaswell2813 Misunderstood. So where did the engine originate?
@paulcaswell2813
@paulcaswell2813 4 жыл бұрын
As with so many of the LNER Pacifics, 532 was named after a racehorse. Blue Peter, owned by Lord Rosebery, won the 1939 Derby and 2000 Guineas. The locomotive (Doncaster works 2023) entered service in March 1948 and carried the name 'Blue Peter' from new.
@mop714
@mop714 4 жыл бұрын
@@paulcaswell2813 Thank you Paul for the info. My dad may or may not have had any dealings with Blue Peter. He was part of the team, but did not come back from WW2 until 1946, so I suspect he may not be involved with it. Interesting.
@paulcaswell2813
@paulcaswell2813 4 жыл бұрын
The BBC children's magazine, Blue Peter, 'adopted' the loco in the 1970s. Maybe that's what you were thinking about...
@Willysmb44
@Willysmb44 5 жыл бұрын
Good grief, that went on for quite a while, much longer than I would have expected after reading the description of the event. That would have been nightmarish to have been standing near the head end on the ground when it occurred! Note the sparks around 1:33, I assume from driver contact with the rails?
@SkyFire2112
@SkyFire2112 5 жыл бұрын
The railway series story: High Speed Gordon was based off this incident
@KorraDaTrainBuff
@KorraDaTrainBuff 5 жыл бұрын
No it wasn't. That book was published 7 years before this happened.
@JohnGeorgeBauerBuis
@JohnGeorgeBauerBuis 5 жыл бұрын
Just for the record, the fastest wheelslip ever confirmed was a deliberate 160Mph with a New York Central Hudson.
@Dockhead
@Dockhead 4 жыл бұрын
so this was 2nd?
@paulcaswell2813
@paulcaswell2813 4 жыл бұрын
And remember that the A2 was a mixed traffic loco - not even an express design.
@mcguireshepherd
@mcguireshepherd 5 жыл бұрын
LNER Peppercorn A2 Class 60532 Blue Peter 1994 accident: On October 1, 1994, during the first run of a preserved steam locomotive from Edinburgh to Newcastle and York, 60532 suffered extensive damage during a catastrophic uncontrolled wheelslip. During an unscheduled stop at Durham station, the inexperienced footplate crew overfilled the boiler. As the train departed south across Durham viaduct an initial slip was poorly controlled by the driver, who then reopened the regulator too early, probably worried about stalling on the bank up to Relly Mill. The force of the initial slip caused the boiler to prime, carrying water over into the regulator valve and jamming it open. This allowed passage of steam through to the cylinders, perpetuating the slip and accelerating the driving wheels. When the driver attempted to wind the reversing gear back into mid-position to halt the slip, the force of the motion spun it into full-forward position, and the driving wheels reached a rotational speed of 140 miles per hour before the cylinder covers blew off and the motion disintegrated. The driver suffered major injury to his arms, as a result of the screw reversing lever whipping around when he released it. The accident brought to light the importance of train crews being trained on the specific locomotives they were driving, rather than simply a common general instruction on steam locomotives. Neither the driver or fireman had ever worked 60532 before, and were unaware of the locomotive's sensitivity to priming, which led to the accident. Source: Wikipedia.com
@thomashambly3718
@thomashambly3718 3 жыл бұрын
I'm going to assume the covers blew off during the video when the train became engulfed in a cloud of steam, correct?
@Gabriel-he6ih
@Gabriel-he6ih 3 жыл бұрын
@@thomashambly3718 bingo, you can even hear it tear apart
@angrya4pacific738
@angrya4pacific738 6 жыл бұрын
I bet you could hear that all over Durham
@Danny-lm9xk
@Danny-lm9xk 4 жыл бұрын
Yes apparently it could be heard all over the town. My dad remembers being at his school and hearing it.
@derekheeps1244
@derekheeps1244 3 жыл бұрын
Gives a new meaning to the phrase Durham Dash , long before Dominic Cummings did his !
@gregkiteos1936
@gregkiteos1936 19 күн бұрын
​@@Danny-lm9xk It was a Saturday that day.
@JamesDTapley
@JamesDTapley 6 жыл бұрын
Who let Jeremy Clarkson on the footplate? Power!
@poly_hexamethyl
@poly_hexamethyl 6 жыл бұрын
Does it really help to run the wheels that fast when they're slipping? I would think that once they start slipping, turning faster won't give much more traction force. Wouldn't they have been better off to run it just a bit faster than when they first started to slip?
@markturner4219
@markturner4219 6 жыл бұрын
It wasn't intentional. The regulator stuck because the boiler was over full and the driver tried to put her in neutral but there was so much pressure that the reverser span into full forward gear. Nothing the crew could do about it once at that stage.
@andrewsmith6563
@andrewsmith6563 6 жыл бұрын
Hey. May I please use some of your footage in my films? I will credit you for it.
@mcguireshepherd
@mcguireshepherd 5 жыл бұрын
This isn't this guy's video. He said in the description, that it is not his video. He doesn't know who shot the footage, but he does give credit for the person that took the video.
@MB_Videos1
@MB_Videos1 6 жыл бұрын
Great video and I would say this is a great opportunity to add some engineering controls that would prevent this from happening again! we have great men that can repair or rebuild anything.
@jeffburch5903
@jeffburch5903 2 жыл бұрын
Yes, a turbo encabulator 😁
@sleeming88
@sleeming88 6 жыл бұрын
Did the safety valve open automatically due to a sudden rise in boiler pressure after the cylinders failed or did the crew open it manually (if that's possible) to vent the boiler once they knew the loco was dead?
@Rosie6857
@Rosie6857 6 жыл бұрын
(sleeming88) The crew can't affect the action of the safety valves in any way. The steam flow during the slip must have been colossal and this would have given the fire a tremendous boost and the loco must have maintained boiler pressure. As soon as the steam flow ceased the still-hot fire would have temporarily raised the pressure very quickly so off go the safety valves. This was a normal occurrence during steam days if the pressure was well up but under rather less insane conditions of course. I wonder how much of the fire was left. I also wonder how much water was left in the boiler after that horror show. BTW you can't empty the boiler without first dropping the fire which is always a priority.
@markturner4219
@markturner4219 6 жыл бұрын
My understanding is the boiler was overfull, which was the root cause of the events that followed. At least with the modern rocker grates that Peppercorn put in they could dump the fire quickly.
@olly5764
@olly5764 5 жыл бұрын
@@markturner4219 not that dumping the fire would have achieved anything
@paulcaswell2813
@paulcaswell2813 4 жыл бұрын
The massive loss of steam looks to me as although the 'lead plugs' dropped. These are a 'last resort', put in a boiler should pressure rise even more than the normal safety valves can cope with.
@KrisDouglas
@KrisDouglas 3 жыл бұрын
@@paulcaswell2813 that's not what they're for. The plugs are a warning device to alert you that the water level in the boiler has dropped below the crown of the firebox. Something that did not happen in this case.
@BoleDaPole
@BoleDaPole 6 жыл бұрын
Didn't know they had cell phones "back then"... clearly faked to make the Queens Country look bad
@scrambledmandible
@scrambledmandible 4 жыл бұрын
Ever heard of a Camcorder?
@mbak7801
@mbak7801 3 жыл бұрын
UK had cell phones (mobiles) in 1983/4. OK engineering sets. By 86 they were common. 1994 everyone and his dog had one.
@nickelplateroad7655
@nickelplateroad7655 6 жыл бұрын
1. Well... shit 2. What did they mean by came off the viaduct? As in it fell right off the tracks or it just derailed or it tipped over?
@shroomzed2947
@shroomzed2947 6 жыл бұрын
It stayed on the rails the entire time. Wheelslip and resultant jammed regulator is what you're seeing here.
@RCassinello
@RCassinello 6 жыл бұрын
Nothing as dramatic - they just mean as it came off the end of the viaduct, still on the rails.
@simon201063
@simon201063 7 жыл бұрын
I've watched this video several times now over a few years and this is the first time I've noticed the sparks coming off the driving wheels. Absolutely red hot. Wow. Just wow.
@beeble2003
@beeble2003 Жыл бұрын
Sparks don't imply that the bulk of the wheel itself is red hot. A spark is basically a small fragment of extremely hot or burning metal. The tiny fragments (potentially just dust) are extremely hot, but the wheel itself isn't _that_ hot.
@camjkerman
@camjkerman 7 жыл бұрын
I'm 14 and I have the solution to that, shut off steam and apply full brake, the steam stops sending pressure into the cylinders so the controls have to more power to drive the wheels and applying full brake will stop the wheels themselves.
@markymark1402
@markymark1402 7 жыл бұрын
camjkerman unfortunately the loco picked up the water and the regulator couldn't be closed. Applying the brakes at this point would be ineffective and only have the potential to cause more damage.
@olly5764
@olly5764 5 жыл бұрын
The loco had picked the water up causing the regulator to jam, meaning steam can't be shut off. Applying the brake with the wheels slipping that fast can cause the wheels to stop at different times causing the axle to twist or snap, causing more dammage, and with that much force on the motion, winding it back to mid-gear is fraught with danger
@paulcaswell2813
@paulcaswell2813 4 жыл бұрын
HA HA HA. Try learning about steam first (and not kids' theoretical 'this is how a steam loco works' books)...
@60103FlyingScotsman
@60103FlyingScotsman 7 жыл бұрын
the aftermath of this accident was all motion was bent beyond repair her wheels damaged cylinders cracked frame damaged and crewmen seriously hurt
@markturner4219
@markturner4219 6 жыл бұрын
Motion wheels and axle boxes damaged. Drivers' finger broken. although soem reports say his arm was broken because it was caught up in the rapidly spinning screw reversing lever which he unlocked when he realized he couldn't close the regulator.
@class87fan54
@class87fan54 8 жыл бұрын
I hope BR were forced to pay compensation to NELPG for the damage their crew caused to Blue Peter. BR should have known that steam loco's are very individual, but they just told a crew with no experience of an A2 to drive her, without giving them proper instruction. The driver was given wrong advice on how to handle her, and this was the result.
@deeremeyer1749
@deeremeyer1749 6 жыл бұрын
Try building locomotives that aren't disasters waiting to happen with shitty "regulators" and a tendency to "prime" along with being lightweight slipping pieces of shit that are either damn near slipping or damn near stalling at all times.
@CrisisOnACanoe
@CrisisOnACanoe 4 жыл бұрын
In inexperienced hands, any locomotive is a disaster waiting to happen.
@Train-Sim-Drives-UK
@Train-Sim-Drives-UK 4 жыл бұрын
A your proof please?
@thomashenderson3901
@thomashenderson3901 3 жыл бұрын
@@deeremeyer1749 Sounds like fun!
@StrawberryStationMusic
@StrawberryStationMusic 3 жыл бұрын
@@deeremeyer1749 *cries in Bulleid*
@thomasweekley9209
@thomasweekley9209 8 жыл бұрын
I'm sure a lesson was learned from that day. Always make sure that the crew is trained before letting them drive the engine.
@TomFromYoutube
@TomFromYoutube 6 жыл бұрын
They all got trained.
@zrspangle
@zrspangle 5 жыл бұрын
@@TomFromKZbin on the wrong type of engine
@Sebdamememan
@Sebdamememan 4 жыл бұрын
@@zrspangle its was not their fault, it was common for the A1 locomotives for the water on the boiler to serge forwards, and if This happends the throtle and reverser cant be closed, it more of a flaw on design than a flaw on the driver side
@zrspangle
@zrspangle 4 жыл бұрын
@@Sebdamememan I never said it was the crew's fault, they weren't made aware of the flaw, so they were just doing their jobs.
@Sebdamememan
@Sebdamememan 4 жыл бұрын
@@zrspangle you didnt but the other guy did
@espeescotty
@espeescotty 8 жыл бұрын
It was told in a video that this also happened to one of the Union Pacific's Big Boys and that it cut through the rails.
@wharris302
@wharris302 8 жыл бұрын
A UP BB doing this? Fucking hell
@espeescotty
@espeescotty 8 жыл бұрын
I watched the video again today. It is in the Pentrex video Last Of The Giants Volume 3: Sherman Hill. In the video they interview engineers and firemen that worked on the Big Boys and one told of the throttle of a Big Boy getting stuck and couldn't be shut off, and that it cut through the rail. The only other specific detail given was that it occurred at Borie, Wyoming. No engine number or year was given.
@deeremeyer1749
@deeremeyer1749 6 жыл бұрын
Obviously the train was moving if the throttle was open and if the train was moving and the throttle was open on a Big Boy, it's going to keep whatever was moving moving and not "cut through the rail". DP units in the mountains can get "stuck" in notch 5 or 6 if the "trailer" loses communication with the leader going over a hump and especially with tunnels/turns and if the engineer sees the lost communication and goes "by the book" to see what's going on like the book says but the FRA book instead of the smart train handling book and he just goes into dynamics and stops quick while the front end is still pulling pretty hard dragging the back end over and doesn't go into emergency because if he DOES get comms back someone still has to go reset the emergency in the trailer, he can end up with a trailer back there in notch 5 or 6 pushing like a sumbitch until the melting rail gets hot enough to get "sticky" and one or more traction motors start slowing down and throwing speed difference/locked axle faults and the unit shuts down 2 traction motors on one truck or one on each truck and safety's out. Especially if he just makes minimum reduction that the rear locomotive might not even "see" in its brake pipe pressure setting because being at the other end of the train that minimum reduction at the front end might only be half as much at the rear and when it's still in a throttle notch and its brake handle is still in handle off and its main reservoir is still good and such and last it knew for SURE its leader was still in Notch 6 and maybe it just saw Notch 5 "flash" for just a second before comm loss, it's back there pushing. Don't take long for 216 tons of GE AC power to spin down through the rail but they only go so far and then they kick out or possibly before sending the conductor for a walk they shut down the lead units. You can hear a GE in Notch 6 maybe 110 cars behind you but only 75 or so as the crow flies because of a curve and maybe a hill pretty easy. And if you hear it powered, the damage is done. Pull the emergency brake handle and it'll keep running at least half-throttle for 15-30 seconds because that's built-in breakaway protection but then it should go to idle. It usually doesn't do anything to locomotive wheels. Those bastards are so hard it takes carbide cutters on the wheel true machine to profile them and you can take a few tenths of an inch per revolution max. Rail is really soft by comparison, lol. Especially once it starts glowing. It doesn't happen much but it does happen and to guys doing it "by the book". That's one situation where you break the FRA rules and if you lose comms you slowly notch down but keep some power on and make a full service application. That'll definitely drop the brake pipe at the back end enough for it to know the brakes came on and notch down or go to idle and to make sure you notch down all the way, ease into dynamics and then go to release. When you go to release that trailer will drop main reservoir pressure as it starts helping pump the brake pipe back up and GEs have electric air compressors and they take a couple hundred horsepower to start and then drop off to 50 or so when they're pumping. That combination of events will kick it into idle or at least pull enough power out of it that it's not going to spin the wheels and if it sits there with released brakes and rising main reservoir and some throttle on but no traction motor is turning, it'll safety out and set a locked axle fault on the motor that's getting the most juice and has the smallest wheel diameter programmed in (most torque output) and if cutting that motor out doesn't free up enough power to turn something it'll cut the next one in line and if they're both on the same truck or one is on each truck it'll go offline all by itself. Or you keep creeping along slowly and keep your hands off the brake and dynamic handles and just let it crawl and "think" and eventually it's going to bounce a signal off the right rocks or a weak one will get through enough for it to see a "mismatch" and the trailer will go to idle then, too. But you've still got your connection. The leaders road number is programmed into the trailer and vice versa and they're both set on one of the half-dozen or so DP frequencies and they'll ignore everything else and as long as you're rolling you're not digging holes. It might be back there spinning but it won't do that for long either. It knows how many motors are online and how much HP it's making by the amperage and voltage and it knows how many traction motor rpm that should equal at a given throttle notch and if it's too high, it'll throw faults and if its too low and isn't increasing, it'll add power to the max for the notch and something will spin or speed up or stay the same and if things stay the same then it "thinks" its just working hard and it'll keep working hard. That's a change they had to make in the DP software because when UP started paying fuel savings bonuses to engineers some of the guys who knew a little about the DP systems would throttle up and get up to whatever speed they were going to run uphill empty heading west across Nebraska and especially from North Platte to Cheyenne or Morrill and then they'd kill the DP radio and leave the trailer back there pushing like a sumbitch and notch back the leader and MU units a notch or two and save ALL KINDS OF FUEL. Because they only kept track of how much fuel they put in the leaders to do their fuel consumption checks. Kinda hard on those old 7FDLs trying to push a whole train in Notch 7 or 8 while the leader is in 6 or 7, lol. And in the Rockys where the comms losses could end up with a spinning locomotive sitting there digging holes they started putting two units on the head and a pair of DP units mid-train so if THOSE somehow ended up "stuck in gear" in a comm loss situation they were going to move something, lol. And having them that much closer made a hell of a difference. Kept the BP pressures much closer together and helped make sure the trailers got the "message" even with a minimum reduction. Of course that only left the train crew with one spare "outhouse" instead of two and they started checking fuel in the leader and the front DP unit too. Of course good train handlers save fuel the way good truck drivers and anybody who knows how to get good fuel economy with any vehicle does. Don't speed up just to slow down just to speed up. A steady 50 mph will get you someplace exactly as fast and with less fuel than "averaging" 50 mph over the same distance spending half your time at 60 and half at 40.
@AMOGLES99
@AMOGLES99 5 жыл бұрын
I think with two sets of motion working independently, the risk is actually quite great that this could happen. I don't know if the BiGBoys had any safeguards to prevent that.
@KrisDouglas
@KrisDouglas 3 жыл бұрын
@@deeremeyer1749 you write a lot but this can happen when pulling off, any locomotive is capable of this (modern locos with "traction control" excepted). A big boy stuck with the regulator wide open would eat through a rail with little effort due to the weight on the drivers.
@susanball8222
@susanball8222 8 жыл бұрын
just glad she has a new home at crewe and may be back in steam like flying scotsman
@m1pete
@m1pete 8 жыл бұрын
It's the same thing has when a diesel engine desides to have a run away, you can't stop it until something breaks..
@SteamTech_4468
@SteamTech_4468 8 жыл бұрын
If the driver had been able to shut the regulator or get the engine into mid gear it would of almost completely stopped the flow of steam which would of stopped the slip but the regulator was jammed open by the water and the engine refused to forward gear.
@deeremeyer1749
@deeremeyer1749 6 жыл бұрын
You can if you know what the hell to do and when to do it. Shut off the air. They stop.
@KrisDouglas
@KrisDouglas 3 жыл бұрын
@@deeremeyer1749 shut off the air?? Its a steam locomotove, it had water locking the regulator open, there have been reports of when this happens that it takes the strength of two to shut it again.
@vinniecross1092
@vinniecross1092 3 жыл бұрын
@@KrisDouglas he meant the diesel engines as referred in the comment, you stop a diesel running away by shutting off the air
@mbak7801
@mbak7801 3 жыл бұрын
@@vinniecross1092 Would you want to get close enough to do that?
@trainmaniacstudios8216
@trainmaniacstudios8216 8 жыл бұрын
1:48 Oooohhhh that sounded painful.....
@Wally34070
@Wally34070 8 жыл бұрын
broke both of the drivers arms
@SirFloofy001
@SirFloofy001 6 жыл бұрын
No broke a finger.
@o.m.b.demolitionenterprise5398
@o.m.b.demolitionenterprise5398 3 жыл бұрын
@@SirFloofy001 “The driver suffered a major injury to his arms, as a result of the screw reversing lever whipping around when he released it.” Broke both his arms.
@nathan83699
@nathan83699 9 жыл бұрын
she is currently at Crewe DMD
@SonicDashie759
@SonicDashie759 9 жыл бұрын
can someone please explain to me what happened but in a way that a 10-15 year old could understand? I'm not the brightest...
@olly5764
@olly5764 9 жыл бұрын
+SonicDashie759 basically the engine lost grip on the track, probably because the rails were wet. As the wheels began to slip, water from the boiler got the wrong side of the regulator valve so it wouldn't close, meaning the slip got more violent until the engine's motion (The rods on the side) thrashed it's self to pieces. Hope this is a straight forward enough explanation.
@Rosie6857
@Rosie6857 9 жыл бұрын
+SonicDashie759 The driver opened the regulator too far and the wheels lost their grip, like a car on an icy road. Well, you just take your foot off the pedal. But regulator handles are not like car pedals - they don't just spring back - they need to be heaved shut just as they need to be heaved open. The regulator is a long handle that is often quite stiff. In this case the regulator could not be closed once the slip had started because of the tremendous flow of steam which dragged loads of water with it. But that's not all. The crucial point is that the water got into the cylinders where there is only a very small clearance (less than half an inch) at the end of each stroke and water is incompressible. The pistons in effect were slamming into a brick wall at each stroke with the result that all the rods got bent and the ends of all three cylinders were cracked, which explains the huge clouds of steam roaring out of the front of the engine. The slip only stopped because the valve gear had got so badly bent that the timing was lost. The driver had no more than a second or two to react and slam the regulator shut before the slip really got going and but it seems he wasn't quick enough, poor fellow.
@Rosie6857
@Rosie6857 8 жыл бұрын
+mighty Kirby That may have been tried but the regulator was probably full open or nearly so anyway. I suspect the regulator could'n't be moved at all against the huge steam and water flow once the slip had got going and that all that could be done was to try and wind the reverser into mid-gear by which time the slip had done its damage. In steam days on BR this never happened, as far as I know, the crew always managing to shut the regulator before the loco was damaged though there was sometimes damage to rails.
@renegadeoflife8774
@renegadeoflife8774 8 жыл бұрын
+Rosie6857 No, he reacted accordingly- but the boiler had primed and jammed the regulator wide open. He then tried to stop the engine by moving its timing to neutral instead of forward- but by then the engine was pounding so furiously that it lashed the mechanism backwards and broke his arm, coming to rest wide open. From there only two things could have stopped it- the engine flying apart from running as flat out as steam can possibly get, or the boiler running out of steam. In this case, the engine literally flew apart. Blue Peter was laid up for months while it was rebuilt.
@renegadeoflife8774
@renegadeoflife8774 8 жыл бұрын
+SonicDashie759 I'm assuming you are familiar with a car doing a burnout- intentionally making its wheels spin on the road by hitting the gas really hard. What happened here was the driver gave the engine a little too much steam and the engine spun its wheels, accidentally though. They recovered, but then opened it up again far too soon. The valve controlling the steam to the engine got stuck wide open, and the engine again lost its grip on the rails. Then in an effort to stop it, the driver tried to put the engine in neutral. On a car this would only let the engine run faster- but steam engines don't have gears, they change direction by changing the timing of the engine. Instead the runaway engine yanked the controls the way it wanted to go, breaking his arm in the process. It ended up flat out in both pressure and timing, with no grip on the rails and going as fast as it could possibly go until it broke apart.
@Stas99able
@Stas99able 9 жыл бұрын
До-катались буржуи - "лошадь" сдохла :-)
@raymondleggs5508
@raymondleggs5508 9 жыл бұрын
cockroach2008 did this
@madrabidfireman
@madrabidfireman 7 жыл бұрын
Is that ass still around?
@whoohaaXL
@whoohaaXL 7 жыл бұрын
"Blah blah blah, cut up steam! blah blah blah" - Cockroach2008....any steam video. He probably turned himself into a quadriplegic with a cutting torch.
@davidantoniocamposbarros7528
@davidantoniocamposbarros7528 3 жыл бұрын
@@madrabidfireman i think so
@gregkiteos1936
@gregkiteos1936 10 жыл бұрын
It took 18 months to repair the damage and Blue Peter returned to main line service in November 1996. She ran from Edinburgh to King's Cross for a 40th anniversary special of the eponymous TV programme. Main line certificate expired in 2001 and she remained at the North Yorkshire Moors Railway until the end of its 2002 season. The latest news is that she's been bought by Jeremy Hosking and will hopefully be running on the main line again by 2020.
@thurstablelane7567
@thurstablelane7567 9 жыл бұрын
She goes in for overhaul this year
@ESSAErin
@ESSAErin 4 жыл бұрын
2020 well that won’t be happening
@NathanielKempson
@NathanielKempson 3 жыл бұрын
2020 here. Uh, good luck with that XD
@gregkiteos1936
@gregkiteos1936 3 жыл бұрын
Will be back this year.
@BreoSims
@BreoSims 2 жыл бұрын
2022 don’t see it
@thedarknessofknight6440
@thedarknessofknight6440 10 жыл бұрын
Rule 1: never use inexperienced crew on such sensitive engines.
@danielpizzey212
@danielpizzey212 3 жыл бұрын
right you are if they want to drive steamengines on the mainline they need to have done 2,000 hours on a steam engine
@gwrstudios5181
@gwrstudios5181 3 жыл бұрын
What I think is maybe the railway didn’t have any experienced crews and had to put them into the footplate and didn’t tell them about her being sensitive
@thewelshtraingeek4895
@thewelshtraingeek4895 2 жыл бұрын
They were relatively experienced, just had never driven that specific loco
@ThatE4
@ThatE4 Жыл бұрын
If you have an uncontrolled and unstoppable slip, cant really do much to prevent it
@steamingaroundbritain
@steamingaroundbritain 10 жыл бұрын
Ouch as soon as i heard what happened to the driver when he tried to wind the valve gear back to norm but it swung back violently thus whipping round the drivers arms and braking them i just heard him screaming in my head
@Tahirah8
@Tahirah8 9 жыл бұрын
kieran evans The driver broke a finger and not his arms. I learn't this recently but it is from one of the other drivers apparently.
@jsma9999
@jsma9999 10 жыл бұрын
There 50,000+ pounds in damage I think ,Tow back where to be fix so No more runs that year
@edifyguy
@edifyguy 4 жыл бұрын
No more runs for 18 months means the loss of income was likely FAR more than the cost of the repair.