I was part of that crew, the pressure relief valve on the inside cylinder opened, and put a lot of atomised oil down to the track, and cause her to slip. The driver did his best to recover, and when we came to a stand, the loco was in top dead centre, so we had to roll back a little bit. From this point forward, the driver concentrated on the regulator and reverser, and i was operating the leading sanders. Once we were on the move, the driver had full control, and kept the momentum going, rather than trying for out and out speed. He did an excellent job in recovering the situation. The firemen (2 on board) also worked hard and well, and we estimated that they shovelled about two tons of coal, to get to the top of the bank. Recovering a train, on a 1 in 40 incline with 6 on, is not easy with a big wheeled express loco.
@iskra12346 ай бұрын
It was undoubtedly the right decision to concentrate on maintaining traction rather than going for speed. Excellent job getting the loco going again, and thank you for the spectacular entertainment!
@volvomad6 ай бұрын
Was it fixed on arrival at the next stop or removed from service for repairs?
@hellotractor47726 ай бұрын
Bet the fireman couldn’t shovel it in quick enough
@iskra12346 ай бұрын
It continued in service on the flatter section of the line without incident for the rest of the day
@7007GreatWestern6 ай бұрын
Thanks for taking the time to explain to us the issues you encountered and the steps you took to manage a very difficult situation. All sorts of people can speculate from the comfort of their armchairs but you were actually there and *know* what happened. . Sounds like excellent Enginemanship. Well done!
@crompton330226 ай бұрын
Thank you for sharing with us. A great performance overall.
@steveevans62416 ай бұрын
I've driven a couple of big steam locos under different conditions & the melding of man & machine is difficult to achieve so the crew did very well here it's a real art keeping things going in circumstances like these.
@davidcrc91556 ай бұрын
The last time i went up this branch line was behind a Fowler 4MT 2-6-4 Tank loco on one of the best railtours I've ever expirienced, 'The Stafforshire Potter' circa 1966/67. We had 5 old LMS coaches, porthole type.
@iskra12346 ай бұрын
That’s a wonderful memory thanks for sharing!
@duck19466 ай бұрын
Well handled loco good job done! Love the stack talk!!
@pjd73256 ай бұрын
Nice to hear the usual "Experts" commenting on the Crew and locomotive performance. It does seam to be leaking a lot of steam from the front end for a recently overhauled locomotive
@doughunt96216 ай бұрын
As the steam from the cylinders apeared to reduce considerably at the end of the video, I would suggest that the cylinder drain cocks were open for much of the climb, then closed at the summit.
@316CactusJack6 ай бұрын
Anything that comes out of didcot does that, the star, 6023, this
@Gary-cvr236 ай бұрын
No wonder we were waiting for her for ages at apesford she also delayed one of the s160s for what seemed like ages awsome footage too
@markburgess45286 ай бұрын
Good recovery but when it started slowing down, was the regulator wide open? I did hear any increase in the exhaust noise. Also no sanders? Edit. Always wondered how a 3 or 4 cylinder engine can get stuck TDC.
@james426able16 ай бұрын
I can't see the staff behind the scenes re inviting the castle back the gradients are too steep for the old girl 😅
@wgj48136 ай бұрын
This is what steam rides are all about lots of steam and sound and the occasional unexpected "bonus?"
@iskra12346 ай бұрын
Couldn't agree more!
@robertmarshall65786 ай бұрын
Wow - what a slog for this express loco! Excellent video. I'm intrigued to know what the crew were preoccupied with during the climb, hanging out of the cab and staring downwards - injector? sanders? just hoping for no more slipping?
@maartendelandmeter77056 ай бұрын
finding a way to see the track and signals into the mist from the leaking glants, leaky bump!