The rebuild of my head and motor after jumping time in my 2010 GMC Terrain
Пікірлер: 17
@dosgos8 ай бұрын
Dorman has a "timing chain guide bolt replacement" 917-954. They have a "case study" and video. Not sure if the Dorman bolt is preventative maintenance. Is the the failure is from OEM tensioner, oil sprayer, cheap plastic guides, bolt, etc. I read that the tensioner and oil sprayer were upgraded in replacement kits. Regardless, might not be a bad idea to check the bolt is tight (I suppose that is easiest taking off the round cover). If one installs the Dorman bolt, I'm not 100% sure if the tensionoer should be loosened and redelployed (which require removing the valve cover).
@factoryratgarage8 ай бұрын
I installed the replacement tensioner bolt. It’s a better design and like it.
@dosgos8 ай бұрын
@@factoryratgarageThanks, I just saw that on the next video. Do you think one could install the bolt as prevention without messing around with the tensioner?
@factoryratgarage8 ай бұрын
@@dosgos I would say it’s possible but if you pull the bolt out the chain will tighten from the tensioner, so I would say if you do it I’d recommend taking the timing cover off to release the tension on tensioner.
@dosgos8 ай бұрын
@@factoryratgarageThank you! This is a great 2.4 rebuild series.
@factoryratgarage8 ай бұрын
@@dosgos thank you
@Rscmgw23 Жыл бұрын
Did you put new rod and main bearings in or just reuse the old ones? Also, what did you gap the rings at? Is the engine still consuming a lot of oil? Never seen someone ring slap an engine without at least ball honing it first.
@factoryratgarage Жыл бұрын
Same rod and main bearings, they had almost zero wear. I can’t remember the gap, I know when I checked them they were spot on so no filing. There was still good cross hatching so didn’t see the need. Runs good everyday since the rebuild and uses no oil.
@xTheunknowntuberx Жыл бұрын
Did this fix your issue still today?
@factoryratgarage Жыл бұрын
Yes still running good today.
@xTheunknowntuberx Жыл бұрын
@@factoryratgarage Thats great to hear. My 2010 with 120k skipped time and smacked the head. Tearing it down now to see how back but borescope showed not too much damage to the piston.
@factoryratgarage Жыл бұрын
@@xTheunknowntuberx good luck I’ll try to help if I can.
@xTheunknowntuberx Жыл бұрын
@@factoryratgarage Thanks for the offer. I'll keep you posted
@xTheunknowntuberx Жыл бұрын
@@factoryratgarage so I got the head off and bent all 16 valves but overall head and pistons looks ok, if done uglier broads. What did you use to clean the mating surfaces and the carbon out of the head.