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The drone crash occurred in active track mode. The obstacle avoidance function was turned on, but the drone did not see the wires. As a result of the crash, a crack appeared on one propeller. Other damage was not.
And by the way, there was a very bright sun that day. I had to use an nd32 filter. But it turned to be light. Nd128 would be just right for recording parameters to be 1/30 at 60 fps and ISO100.