Did you try tying a string between that chuck and the door knob? Slam the door shut, and it should have popped right out. 😊
@user-jr2ue9nu6y7 ай бұрын
ROFL like my tooth as a kid
@RotarySMP8 ай бұрын
Hi Jeremy, Love your version of gardening with the needle de-scaler and plants.
@michaelallen14328 ай бұрын
Had to do it sooner or later. I was totally holding my breath as you were boring that out. Literally at the point where I was thinking "ok, time to stop and just buy a reamer", you stopped and bought a reamer. 🤣 I was actually expecting you to find significant damage to the surface inside. I was thinking there was a good chance that it had spun in the taper and friction welded itself in place. But it looks like it just had some corrosion. Thanks for showing not just what went right but what went wrong. That helps those of us watching avoid wasting our time on simple mistakes, so we can instead waste our time on new and innovative mistakes.
@Mrcaffinebean8 ай бұрын
First time viewer here. The second you chucked an old drive shaft into your lathe I became a subscriber. My kind of guy!
@Blondihacks8 ай бұрын
Nice work on repairing that spindle! That was a difficult operation.
@JeremyMakesThings8 ай бұрын
Thanks Quinn!
@tadamb18 ай бұрын
You missed the opportunity to pretend the fly cutter got stuck in the spindle at the end of the video. Otherwise, quite interesting. Can't wait to see more of the Jeep project.
@kglesq18 ай бұрын
That was great from beginning to end. I love the use of 'junk' material to build useful things. BTW your narration is excellent. Subscribed.
@scroungasworkshop46638 ай бұрын
Well done Jeremy! If it’s any consolation it took me 20 years to finally get the screw on chuck off my lathe. Cheers mate, Stuart 🇦🇺
@1crazypj8 ай бұрын
I never got the screw on chuck off my Colchester, ended up selling it with it still stuck (did some major turning with intermittent cut that tightened it up way too much) It did make enough money to pay for the lathe though plus, I couldn't ship it 4,500 miles
@Pappaoh8 ай бұрын
My comments are as follows: 1 excellent project and sub-projects. As a fan of your channel, I knew this day was coming, and I'm so glad you fixed that old machine rather than doing the sensible thing. 2. Your use of dog shit material from the river bed never disappoints. That steady rest is Gucci as hell. 3. Your power hair @0:11 inspires me to be a better and more potent man. I mean, I've worked my ass off much of my life, but that hair and those pseudo chops help me see I could be more. Thank you for that, sir, and thanks for another great vid.
@benjefferies71238 ай бұрын
🤣🤣🤣
@ggray20118 ай бұрын
I've been looking forward to this repair since you first introduced the milling machine with the stuck collet chuck. Thanks for sharing.
@Heasyy8 ай бұрын
Thanks for taking the time and effort to make these videos, they are really great and I learn a lot from you.
@charlieromeo76638 ай бұрын
Nice recovery, and I really like the idea of repurposing the axle shafts and other parts. Great job.
@billgilbride79728 ай бұрын
Inspirational! Fantastic finish with all the tooling fixes and such. I feel less worried about my 5c holding devices addiction. Thanks!
@neodimium7 ай бұрын
What was that deflection 1:51?
@TalRohan8 ай бұрын
This is the side project video that finished up with a great flycutter and some other useful stuff. I bet that was satisfying when the last stuck bit came out of the quill , just the cylinder you managed to machine out was awesome. Whenever I have had to spend a lot on a single use tool, I always feel justified when it goes the way it should and even better when it finds other uses ...Ive had my share of wishing I hadn't bought the tool cause something else went wrong right afterwards ....or worse the tool broke.
@amok428 ай бұрын
It must be great being able to use your mill to it's full capability finally.
@jeffschroeder48057 ай бұрын
The joy of the journey is real and the destination turned out to be quite worthwhile as well.
@tuck19638 ай бұрын
I have an INDEX model 45. Searching for info is how I found this channel. Subscribed immediately!
@adeeponionbrah8 ай бұрын
Nice job friend. You showed tenacity.
@chrisbartolo43088 ай бұрын
My Sheldon No. 0 horizontal mill has a B&S 9 spindle and the arbor was absolutely stuck when I got if after sitting for decades. Wedges from opposite sides did the trick easily. Hold a hammer on one side, strike the other and repeat a few times...like separating a drill chuck from an arbor.
@JeremyMakesThings8 ай бұрын
Yep, I tried wedges. The should on the back of the collet chuck was curved and made it hard to get them to seat, so they just bent out ward.
@chrisbartolo43088 ай бұрын
@@JeremyMakesThings I can see that. When you put the carbide in the vise I was thinking you were going to square that up for wedges at first...might have been too much of a gap though for normal wedges. Stuck stuff sucks!
@erik_dk8428 ай бұрын
@@chrisbartolo4308 With the spindle removed, he could put it into a bored throug block, sawed in half, and put one half on an anvil, the other on top, and strike it with a big hammer, turning the spindle in the process. Like when you remove steering ball joints, only the have a much steeper taper. Same principle works for drinking glasses stuck together - hit them on the side with a wooden kitchen utensil, and they come right apart without damage.
@JoeyG19738 ай бұрын
I am constantly lightly cleaning my 55 with my brown and sharp 9 taper. That bs9 taper has done wonders to the spindle accuracy since I got it.
@bwizard79497 ай бұрын
First time viewer, subscribed. Been procrastinating getting my SB 7 shaper operational, you convinced me to man up. . . thanks for taking the time to record, edit, post your work. Good job.
@JohnThawley8 ай бұрын
This is the video I’ve been waiting for. Well worth the wait and even better than expected. Bravo!
@fna-wrightengineering8 ай бұрын
Well done! That was indeed a lot of work, but I feel like this is one of those things that, a couple of months from now, you'll think to yourself, "How the hell did I get on with that collet chuck for so long?" Now the funny part is, you'll probably end up making a new B&S #9 collet chuck for some other project down the road. At least you won't get that one stuck! Also, I get unreasonably excited to see someone using a J.T. Slocomb micrometer. I've got a large collection of them, and rarely see them in the wild. (If you ever need/want to restore yours, I've got a video detailing the process)
@JeremyMakesThings8 ай бұрын
I’ve got two Slocumb micrometers, the other one appears to be older (and has smaller markings on it). It’s one of those tools that, for whatever reason, just has the “right” feel to it.
@melgross6 ай бұрын
It’s frustrating. We’ve all been there. But hey, you got a video out of it! So all is not lost. Keep struggling. I can tell you that the results are much more satisfying when you do.
@peteb27 ай бұрын
Out of all this i have to say i am impressed. It's been awhile since i set foot in my little hobby workshop where i make perfectly good pieces of metal into utterly useless things. And now i am dealing with having had total knee join surgery done by a CNC machine! Subscribed!
@CL053DC45K377 ай бұрын
Man I bet you feel good after all that work. You now have full use if your mill and I'm betting the rigidity is way better now and that is going to show up in your future projects.
@XXLkielbasa7 ай бұрын
Index is still a company. I just lost my index 55 to shop fire by arson. You can send them the quill to clean up the bs9 and cut it for r8, and you can use both types of tools
@brucematthews64178 ай бұрын
At least you made the most out of the setups with the extra tooling. That's a good start towards the eventual compliment of stuff. But yeah, I can just imagine the number of hours bleeding away between beginning and final sigh of relief....
@t0mn8r357 ай бұрын
That was a very difficult and impressive job.
@anandarochisha7 ай бұрын
Did you try turning the mill upside down to let gravity assist You ? 😊
@henrikhv50848 ай бұрын
long time coming, but sure worth waiting for. I think you did a great job, and thank you for sharing ;-) cheers from Denmark
@garyevans98688 ай бұрын
Another great video Jeremy 👍l really enjoyed watching your videos as l find them very informative and entertaining, you seem to be able to make almost anything from nothing but scrap. Keep it up mate, Gary from the UK 🇬🇧
@Trouble-oq4ze4 ай бұрын
Love your recycling program. Enjoy your videoography!
@steamfan71478 ай бұрын
That's my life in a nutshell, 2 hour project turns into 3-1/2 day machine repair saga.🤣
@jeremytodd49068 ай бұрын
Me too!
@christopherbill85378 ай бұрын
1:25 - Scissor-style knurlers are one of those tools that you will not regret making.
@camillosteuss8 ай бұрын
True, they beat the plain knurling tool by a galactic margin...
@canonsonico37528 ай бұрын
Your channel name is real, jeremy *infact* makes things.
@cyclebuster8 ай бұрын
gotta love the model 40. Someday I want to restore mine, but I want a white seamless machine, possibly powder coated. I use mine a lot.
@ollysworkshop8 ай бұрын
Looks like breaking the lathe was the best thing for it, maybe I need to break mine 🤔 looks like the mill is now a whole lot more versatile as well. Doesn't turn out that well very often! Also I love your use of the rustiest piece of metal on the planet to make your drawbar.👍
@JeremyMakesThings8 ай бұрын
“Broken” is a spectrum. It went from “a little broken” to “too broken.” There’s a lot more that’s a little broken that hasn’t forced me to fix it yet.
@ypaulbrown6 ай бұрын
Mr Jeremy, I really enjoyed watching this struggle, your approach seems to be very similar to mine..... if it ain't one thing, it's another, Best Wishes From Florida, Paul
@marcsimonsen15788 ай бұрын
I can feel your pain with that spindle repair!!!
@marvtomson5747 ай бұрын
I had a situation like this one time. For the life of me I couldn't get it out and was getting ready to cut it off, as like here, then I thought about using the rosebud torch to heat it up. And then try knocking it out with a shoe horn wedge and hammer. THAT ACTUALLY WORKED! It deformed the collet a tiny bit and about a month later ended up snapping when it dropped onto the work bench table. Not sure if they are made out of hardened sping steel, one piece cast and formed steel?
@lennyf19577 ай бұрын
6:00 that's steady rest looks like it was discovered in an archaeological dig.
What an adventure! You are a brave one sir. I was on the edge of my seat, even having read about this adventure on Craig’s Workshop discord! Nothing like seeing it, I was so enthralled and just HAD to see the end!
@alangreen58588 ай бұрын
That is the exact same method I used to remove a jammed morse taper sleeve from my mill spindle, right down to buying the correct reamer to finish off the job. Nicely done!
@andrewdolinskiatcarpathian8 ай бұрын
“That was tough”, but oh so worthwhile. Well done for a brilliant result. 👏👏👍😀
@warrenjones7448 ай бұрын
Damn Jeremy, and here I was thinking earlier this week am I the only person in the world that struggles with "everything I own is worn out and has to be fixed to use it". Nice to see I have company! Did you ever determine exactly why the taper was stuck in there in the first place? Nevertheless nice job and now you have full capability restored to the Index. That's worth the time any day! cheers
@JeremyMakesThings8 ай бұрын
From what I can tell from other people’s experience, these tapers like to get stuck sometimes (probably a combination of over tightening and leaving it too long). Even in normal use, it takes some force to get the tool out. It seems like there’s a reason they don’t use this taper any more.
@erik_dk8428 ай бұрын
@@JeremyMakesThings The shallower the taper angle, the harder it bites. Ask any flat bottomed boat owner who's run aground.
@XXLkielbasa7 ай бұрын
I also have a right angle/horizontal head attachment. For index 55. Not sure if it will fit your model. But it’s for sale. Extremely rare
@martindietrich20118 ай бұрын
I hsd a similar priblem in my lsthe. The xhuck was stuck on the spindle nose. I solved the problem with e lobg lever for turning , heating the ouside with a inductive heater an coolibg the inner part with cold spray ....
@therabbits1687 ай бұрын
The cascade of problems is great!😂
@billkirkland80258 ай бұрын
Nice job Jeremy!!!
@MyMiniHomeWorkshop8 ай бұрын
Ah the joys of owning and working with old machines, you got some awesome-looking finishes on some of those parts, nice outcome. 👍
@Calligraphybooster8 ай бұрын
I didn’t check what you did and didn’t try… but my first thought was improvising a firing pin and end cap to fire a blank cartidge on it. (Consider a 1 mm vent hole, use a face screen etc etc and don’t forget a wooden cushion for it to land on in case of success). Anyway… you succeeded as you did and I enjoyed watching.
@larrykent1968 ай бұрын
On my fly cutters I always grind a notch in the bit to put at lest on of the set screw into. It won't slip out. I sure feel safer using it. I have seen them fly out, probably why the call them fly cutters. Cheers!
@junkyardsearcher64078 ай бұрын
Absolutely beautiful work!! You show such a variety of skills, your fun to watch.
@dougmac7778 ай бұрын
That was a lot of work, but I enjoyed it!!! Thanks1
@Cjarka_8 ай бұрын
OOO WEee I was looking forward to this vid ever since you mentioned the collet chuck was stuck you did a way nicer job removing a stuck taper than I did, I cocked up 1/3 of the circumference of the tapered bore but luckily only half way the length of it so it's still plenty precise
@nickkoop44478 ай бұрын
Honestly really happy for you to have gotten your mill spindle back
@rickpalechuk44118 ай бұрын
Anchorlube.... I put that s**t on everything 🌭🌭😁😁
@sacriptex58708 ай бұрын
Dude you actually fixed everything!! Conglatulations! Amazing video and talent
@craigtpat8 ай бұрын
I have seen bushings / bearing housings being removed by welding a few beads on the inside. When the filler metal cools the base metal shrinks. Neat trick. A possible solution after boring out the spindle.
@PuchMaxi6 ай бұрын
Pretty fly!
@Craneman4100w7 ай бұрын
Looks like fun, subscribed
@wizrom30468 ай бұрын
If a tapered fit device spins it can friction weld itself into the receptacle. I think yours might have have a small area welded in, basically you have to machine it out and re cut the female taper (as you did). My big old drill press has a morse taper that refuses to come out for the last few years... hopefully I can get it out without as much work (famous last words) 🤔
@chauvinemmons7 ай бұрын
Don't you love when a plan just comes together
@keithjurena93198 ай бұрын
Had a similar stuck shaft, only this was due to aluminum corroding inside chrome moly steel. Seat post on a bicycle. Tried freezing the aluminum with dry ice and even liquid nitrogen. Ended up dissolving it with sodium hydroxide.
@erik_dk8428 ай бұрын
I tried that in vain
@carlwhite82258 ай бұрын
Jeremy, new guy here and i love your channel, Thanks.
@jacqueso84248 ай бұрын
Your shaper as a backup machine saved you to fix lathe which in turn fixed your milling machind. Good collection, though i wouldnt have gone through the pains of making such a big fly cutter. At the edge of your machine's capabilities? Otherwise great repair job wish i had an inspection camera like that
@rallymax28 ай бұрын
Big win. Congrats.
@Lukedriveitlikearental7 ай бұрын
What lathe do you have it looks like a Logan lathe
@MrEFHATCH19906 ай бұрын
Have you tried gazing at it lovingly?
@JustinMiales8 ай бұрын
Some heat to get that Chuck out or if you can get a thing we use for body work we call it a slap Hammer it's a weight on a slide and you like a hammer you hit it down and it'll pull dents out of the car pull bearings out
@ch34pskate167 ай бұрын
Liquid nitrogen?
@sklarworks31377 ай бұрын
This vid is great! Thanks!
@barthanes18 ай бұрын
Exactly how many pieces of riverbank have you employed in your shop?
@JeremyMakesThings8 ай бұрын
A LOT!
@N.Cognito8 ай бұрын
Wow. It took both of your lathes to get the chuck out. Glad it went well.
@bobweiram63218 ай бұрын
Did you try a torch? The only time it fails for me is when there's a pin somewhere. Btw, you can probably buy a new Bridgeport spindle and quill for not much more than the new reamer.
@JeremyMakesThings8 ай бұрын
I did try a little bit, the two problems with it were: 1) it wasn’t possible to heat the spindle directly, since it was inside the quill (and the bearings) and it wasn’t possible to get the spindle out of the quill with the collet chuck in it and 2) getting the spindle too hot would risk ruining the temper on it.
@digitalradiohacker8 ай бұрын
I have only just come across your channel - Subscribed. By the way, with the awful noises made by the drilling - there is a kind of "toothpaste green" lube that kind of anchors itself to surfaces which seems to help - I forget the name of it just this minute.
@JeremyMakesThings8 ай бұрын
I’ll look into that. 😆
@The-Muninn8 ай бұрын
Great job, thanks for posting. Take care.
@williamfields10218 ай бұрын
I'd watch you for the dry humor alone...
@Rubbernecker8 ай бұрын
I agree!!!
@TgWags698 ай бұрын
What part of your mill did you destroy? Didn't see anything like that. Looked like a good repair and brought it back snuff.
@JeremyMakesThings8 ай бұрын
The collet chuck. It had made itself a permanent part of the mill.
@sjv65988 ай бұрын
I’m assuming giving it a stern talking to didn’t loosen it?
@JeremyMakesThings8 ай бұрын
I asked nicely, I cursed at it, I talked firmly but lovingly to it. I guess I probably should have tried singing to it? I didn’t do that.
@sjv65988 ай бұрын
@@JeremyMakesThings there you go. I knew you didn’t try everything 🙂
@RustyInventions-wz6ir8 ай бұрын
Very interesting. Nice work
@charlescarter74968 ай бұрын
you should use a follow rest on long pieces
@Zzrdemon66338 ай бұрын
I'm assuming you tried a puematic hammer down the draw bar hole? At the same time another hitting it sideways?
@JeremyMakesThings8 ай бұрын
Yes
@Trouble-oq4ze4 ай бұрын
I am so glad to know I am not the only one to have a pair of long nose pliers with a shunted nose. The nose broke, HAD to be ground to an overall symmetrical profile. Just could not get myself to throw them away. The finish on the fly cutter is fine... she may not be the prettiest girl at the Ball, but boy can she....
@sparkyy00072 ай бұрын
Run liquid nitrogen (-196 C) down the drawbar hole to the chuck with a plastic tube to shrink the taper. If you can get the taper to at least -100 C, the taper will shrink 0.0015 inch and should pop. -150 will give you 0.00225 shrink but 0.001 should be enough as long as the taper wasn't spun.
@Watchyn_Yarwood8 ай бұрын
Dude, you never cease to amaze me!
@GoPaintman8 ай бұрын
Totally unrelated: Could you put that slick tapping head you have in the tail stock and use it to quickly tap parts on the lathe?
@JeremyMakesThings8 ай бұрын
I think you could tap with it, but it wouldn’t reverse on its own. I guess you could reverse the the to back it out.
@eternaloptimist28407 ай бұрын
That was funny - broken mill, broken lathe, I thought "next will be a shaper" and sure enough ... I suppose it might have been a surface grinder.
@JeremyMakesThings7 ай бұрын
What is it they say about shapers? Something like “you can make anything with a shaper, especially if your lathe and mill are both broken.” I think that’s how it goes. 🤣
@bruceanderson94616 ай бұрын
It took me a long time to find out if a taper should be lubricated or dry in use. The answer is as dry as you can make it. If you lubricate a tapered drill bit you will bend or break off its tang. This information comes from Boeing.
@pauldorman8 ай бұрын
A tight-fitting copper bar (tapered maybe) that sticks out 5-10 cm inserted into the collet, then submerging the lot in liquid nitrogen might have been an interesting experiment :)
@JeremyMakesThings8 ай бұрын
I’ll give you that one- I didn’t try that, and there’s a (slim) chance it could have worked.
@robertburns24158 ай бұрын
skill is the great equalizer. you have arrived.
@tonyray918 ай бұрын
Well done, I have a pulley stuck on a motor shaft that might get similar treatment today if my 8T home brew hydraulic press doesn’t persuade it to comply.
@erik_dk8428 ай бұрын
The BS #9 reamer costs *$220* 0.9″ Small End, 1.155″ Large End, 1″ Shank, 6-1/8″ Flute, Brown and Sharpe Taper Reamer #9
@Andrew_Fernie8 ай бұрын
That was as stuck as the backplate on my lathe was stuck to the spindle. I ended up turning it off in my mini lathe. That 5" diameter backplate took many hours to get rid of 5 thou at a time 🙄
@CorollaGTSSRX8 ай бұрын
Did you try Liquid nitrogen :)
@juyfjgfjhgfjugf47028 ай бұрын
thank you
@theradarguy8 ай бұрын
When my collet got stuck like that I used a large bearing puller with success.
@martin-vv9lf6 ай бұрын
yep those hydraulic pullers are a deadly animal. sliding hammers are a great thing too. they would produce exactly the kind of shock force that is the opposite to what seated the arbor.
@Unrivaledanime8 ай бұрын
I would suggest calling Dr Gupta he is my gastroenterologist and his fingers are long enough to feel for and remaining bits lol 😂