FPV gear at the ready but unfortunately this is the final flight for the nonacopter. Nonacopter playlist: • Nonacopter Thank you for watching, please consider supporting my work. www.rchacker.co...
Пікірлер: 8
@EnuffsEnuff3189 жыл бұрын
You can hear intermittent rattling on both flights and judging by the intermittent vibration, one or some of the motors might have come loose. You didn't check them after the first flight and I'll bet one of them finally broke away, hacked up the arm, and ditched. Maybe it wasn't a step back in FC's. Maybe the FC couldn't deal with the loose motor? Just a guess.
@Spoif9 жыл бұрын
That was very unlucky. Sorry to see that it was a write-off; but it was a very interesting build.
@Rchacker9 жыл бұрын
I agree with you nuff nuff. Was thinking the same thing as I was editing it.
@rc-wingman57199 жыл бұрын
i think this is great with a camera gimbal and a second operator because you have enough redundancy. Have you ever tried to make a multirotor out of carbon-fiber stripes and join all parts together with rubberbands and tape? Its light and indestructable!
@AntonioSantosDIY9 жыл бұрын
Hey Mark I would like to see a video about openlrsng PPM SUM ( CPPM ) vs Sbus delay on naze32 if possible... or frsky D4R-II CPPM delay vs openlrsng sbus... on the osciloscope and also how it feels while flying, it should 80ms vs 9ms diff
@philippkleeen80139 жыл бұрын
are these Wallabys at 1:30?
@Rchacker9 жыл бұрын
+Philipp Kleeßen Eastern Grey Kangaroos.
@philippkleeen80139 жыл бұрын
+RCHacker pretty cool :) i´m sorry for the crash. looking forward to some more mini quad stuff, though :)