Redemption Dyno!! 393ci Windsor Stroker | 1988 Fox Body Mustang Dyno (Part 2)

  Рет қаралды 5,962

Late Model Restoration (LMR)

Late Model Restoration (LMR)

Күн бұрын

Пікірлер: 40
@ogsuperflygarage
@ogsuperflygarage Сағат бұрын
Great work as usual guys!!
@wolfthornhawkridge5705
@wolfthornhawkridge5705 17 сағат бұрын
Never stop looking for the cause.
@droppedf100
@droppedf100 8 сағат бұрын
Love seeing updates with real world issues and repairs 💪
@mike4fo
@mike4fo 19 сағат бұрын
I love that you guys came back to the car to figure things out. Nice build
@gregbartos9275
@gregbartos9275 10 сағат бұрын
Love it. Yup, that's working on cars for yah! Takes more confidence to say, "yup, I messed up/overlooked something", but what matters is looking into it and figuring out what the true root cause was. Finding the root cause is very rewarding! Especially when, in this case, it means a significant horsepower increase!
@albertespinoza5842
@albertespinoza5842 18 сағат бұрын
Good catch, that's what it's all about,gotta grind before you shine.
@Nondescript15
@Nondescript15 Күн бұрын
That’s amazing. Good catch.
@Bacongrease00
@Bacongrease00 19 сағат бұрын
Custom camshaft and a ported intake manifold would pick up some power if the owner wanted to squeeze out even more. I think 450-460whp is on the table if optimized.
@kennethbrown5784
@kennethbrown5784 17 сағат бұрын
It definitely has more in it
@Bacongrease00
@Bacongrease00 17 сағат бұрын
@ trick flow R lower is probably choking it down a bit. If I recall it flows like 260-275cfm stock form. A bit less than those heads can do. A super victor with an elbow would probably hurt the bottom end a bit but then after 4500 really start to wake up.
@genemounce8302
@genemounce8302 16 сағат бұрын
Merry Christmas from down here in Bertram, TX yall !
@paulhudgins5120
@paulhudgins5120 18 сағат бұрын
Awesome catch, like you said problems are linked to everyone who works on cars. Always trust the butt dyno.
@lwellsfoxbody6491
@lwellsfoxbody6491 19 сағат бұрын
Awesome Find!🔥🔥
@ClickbaitMotorsports
@ClickbaitMotorsports 19 сағат бұрын
Good info. Such a beautiful Fox, oh man. 🔥
@MrCt302
@MrCt302 17 сағат бұрын
Oh Yea!!!!! 👍👍 Still got room for more..
@awee5816
@awee5816 14 сағат бұрын
Can a C4 trans handle this power without having any problems? Or are you going to fix it Now & then with the 393 ci.?
@Olds_Pwr
@Olds_Pwr 12 сағат бұрын
I say yes. Broader Performance seems to be very knowledgeable on these transmissions, may want to watch some of his videos.
@awee5816
@awee5816 12 сағат бұрын
@Olds_Pwr thanks 👍 bud
@Hot_Rod_lincoln
@Hot_Rod_lincoln 16 сағат бұрын
Wow good find! Merry Christmas guys and Landan you guys need to do a dyno video of the new sve heads on a stock(ish) motor and maybe do a comparison to gt40s
@brianwdodge1
@brianwdodge1 16 сағат бұрын
Better! She’s still peaking at a very low RPM (5,300) though. Needs a shorter runner intake. If the peak was close to 6 grand she’d make way more power!
@TexasMarkVII
@TexasMarkVII 18 сағат бұрын
Correct me if I'm wrong, but should a Mass Air setup NOT have an open filter on the oil fill? Is that not unmetered air?
@FourTwentySeven-f7m
@FourTwentySeven-f7m 13 сағат бұрын
It can if the pcv hole is sealed up, vacuum line capped and the sample tube is capped off. Then it’s just venting to atmosphere. Should have a breather on both sides to keep It equal. Good catch btw
@devengudinas1649
@devengudinas1649 19 сағат бұрын
Power
@93_LXcpe
@93_LXcpe 18 сағат бұрын
Max. HP rpm seems a bit low, cam related?
@KingJT80
@KingJT80 18 сағат бұрын
max HP at 5500+ RPM everything doesnt need to make 600 at the wheels. its NA which is good with that size cam and intake and heads
@93_LXcpe
@93_LXcpe 17 сағат бұрын
@@KingJT80 423 @ 5300 just seems a touch low rpm wise, nothing wrong with it. I would take it 🙂
@FourTwentySeven-f7m
@FourTwentySeven-f7m 13 сағат бұрын
I believed they stopped the run there.
@bradnimbus4836
@bradnimbus4836 19 сағат бұрын
Fuel tank problem caused by the same guy?
@MrCobracoupe
@MrCobracoupe 19 сағат бұрын
What’s the rear tire size on drag radials?
@whitetailfox1
@whitetailfox1 19 сағат бұрын
Would love to see this with a vortech supercharger bigger fuel system coil near plug swap and a box r manifold
@kennethbrown5784
@kennethbrown5784 17 сағат бұрын
I had a sump break anytime I got to lower than 1/2 tank it would die in a turn I just lived with it till the s hose busted
@FourTwentySeven-f7m
@FourTwentySeven-f7m 13 сағат бұрын
How many people said it was the pro m EFI system? Wrong as usual.
@hereinmissoula11
@hereinmissoula11 10 сағат бұрын
not sure if it is the cam timing or the intake, but this motor is choked. should not peak and then fall off like that... not at 5500
@catchk9
@catchk9 17 сағат бұрын
Share the combination because better numbers can be made with a 347
@FourTwentySeven-f7m
@FourTwentySeven-f7m 13 сағат бұрын
You show me a video of an na 347 putting those numbers down with off the shelf components and a box stock tune.
@melissaregenwether
@melissaregenwether 19 сағат бұрын
car would benefit greatly from a box r upper. theres a huge casting flaw in the long runner r upper that slows airspeed
@FourTwentySeven-f7m
@FourTwentySeven-f7m 13 сағат бұрын
Maybe but need a different hood and torque would suffer.
@anthonygrebner
@anthonygrebner 3 сағат бұрын
​@@FourTwentySeven-f7m Oh, got ya. So what you're saying is a decrease in horsepower to increase torque is a 21st century secret to going fast. We've all been missing out.
@FourTwentySeven-f7m
@FourTwentySeven-f7m 42 минут бұрын
@@anthonygrebner depends if you want the engine to live at 5500+ guy. A decrease in torque is a decrease in hp. Simple math. What supposed flaw is in the long runner intake?
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