A great improvement to the cross slide. I learn a lot from your videos. I like the why you explain the problem, how you will fix it, then demonstrate the fix.
@WinkysWorkshop2 жыл бұрын
Great to hear! Thanks
@MattysWorkshop4 жыл бұрын
Gday, this made a great improvement to the lathe, the new bolt doesn’t look out of place at all, definitely worth while doing, great job mate, cheers Matty
@WinkysWorkshop4 жыл бұрын
Very true! Thanks Matty!
@t.d.mich.70644 жыл бұрын
Hey Winky! A good way to avoid issues while drilling brass and bronze, is to use a oil stone and stone a little negative rake on the face of the cutting edge of the drill bit. It won't take much and sure makes life easier. Use a little cutting fluid while drilling and you can control the drill bit easily. I used to keep a full set of negative rake drills, taps, and counter- bores for bronze, along with a full set of bottoming drill bits and taps. Thanks for the video as always!
@WinkysWorkshop4 жыл бұрын
Thanks... I definitely should have used oil!
@cooperken114 ай бұрын
Works a treat for drilling Perspex as well
@airgunsfreedom700ssp34 жыл бұрын
Great job Winky. I replaced the nut,s on my mini mill with sintered bronze, and lengthened the nut 1/4". I sacrificed a little travel, but gained stability. For now there is less than a thou backlash which I discovered is in the thrust bearings.
@WinkysWorkshop4 жыл бұрын
Nice work! You almost have to have at least .001!
@jimpritz41694 жыл бұрын
Excellent video and you have a way of explaining things so that when you're done it all just makes sense. Thank you for that.
@WinkysWorkshop4 жыл бұрын
Very welcome Thanks for the comment.
@AdventureswithJane4 жыл бұрын
Fun to watch you work. Excellent shop project. I need to pay more attention to tuning up my machines. Well done. 😎 -Mark
@WinkysWorkshop4 жыл бұрын
Thank you sir! This has been bugging me for a while. I can deal with .005 or even .010" but .040 was way too much.
@trialnterror3 жыл бұрын
I bought a LH acme thread tap for my lathe cause like you I couldn’t find one on eBay. I may make another one after seeing what you’ve done here! Great job
@WinkysWorkshop3 жыл бұрын
Go for it
@TomokosEnterprize2 жыл бұрын
You keep at this you will have a better than new lathe. I am surprised you chose brass. I thought TQ100 hot plate would have been a beter choice. It is highly machinable with great wear resistance. Brass is slippery enough but I suppose the wear has to happen somewhere eh. Either wear the screw or wear the fitting. You made a better choice my friend. You sure solved the backlash and now time will tell all on your material choice. I am thinking your on the money my friend. Hmm, I was always taught to work cast iron dry with min rake on the tools. Same speeds and feeds as stainless. Great results my friend.
@WinkysWorkshop2 жыл бұрын
Brass is easier to machine and better than steel for wear plus it's fairly strong. I'm sure some sort of bonze would be better but I'm not sure what type.
@TomokosEnterprize2 жыл бұрын
@@WinkysWorkshop When I was making silver chopsticks(.925 Sterling)(I have a couple video's on them) It was necessary to toughen up pure silver so the sticks wouldn't bend out of shape when being used. I was originally using copper as the alloy but was having some difficulty with getting the metals mixed so no copper would show. A good friend suggested I use zinc (another soft metal) so I went primarily with zinc and a touch of copper and brass. I had to pour the mix a total of 5 times to get it properly mixed. I am still amazed at how tough the mix was/is. Effort is needed to cut the 1/4 x 3/16 in sticks with a 18 in pair of bolt cutters that if the mix was pure silver a 12 in bolt cutter would easily snip through them. Perhaps a copper/zinc alloy would work for you in this case. It would be easy enough to pour a block of it. Possibly a new project for you when you have nothing else to do, LOL. In the spring I can put a pour of it together for you for fun. It would be great to do a small project together. I would just need an approx. weight and rough casting sizes. I would think an 1/8" on all sides would give you a nice clean piece when finished. I still can't get over how 2 or 3 soft metals will make a really hard one. A while back a pourer called "Backyard Bullion" from England and I did a trade. He did a really nice video on the sticks.
@WinkysWorkshop2 жыл бұрын
@@TomokosEnterprize - Thanks for the offer. I might take you up on something like that in the future but I'm not sure I want to make the nut again seeing as how it works quite well. I think it will likely last too. Brass might not be idea but compared to steel on steel it's much better... likely better that steel on cast iron too... which is what the original was.
@zombieprinting26703 жыл бұрын
Just love when you get excited when things work out perfectly. Learning lots from you, Thanks!
@WinkysWorkshop3 жыл бұрын
Thanks for watching!
@steveforbes8287Ай бұрын
That was fascinating! Excellent analysis and presentation. Thank you.
@WinkysWorkshopАй бұрын
Glad you enjoyed it!
@aeroearth4 жыл бұрын
Great upgrade to the South Bend lathe! I did the same operation of my English Smart and Brown SABEL lathe that is clearly a development from the South Bend lathe. Couple of things spring to mind. When machining cast iron it is usually best to cut it dry, the graphite in the cast iron acting as a lubricant. Listening to the milling cutter it sounds as if it was stop/starting in the cut which the lubricant could have made worse. You can avoid brass grabbing on a drill and pulling it into the cut by grinding a negative rake to the two cutting edges. I made my cross slide nut from phosphor bronze and with no tap to hand, internally screw cut the left hand square section thread. With only the one lathe I had to make a dummy section of male thread to use as a plug gauge when screw cutting the nut. On the SABEL the lead screw nut has a close fitting boss locating in the slide and to clamp uses a slotted head set screw with 45 degree tip that drives out a side pin. The side pin sits in side hole of nut and is radiused one end to match cross slide bore and other end at 45 degrees to bear against conical end of set screw. My set screw slot was worn/damaged so I made a new one. Slot I cut with slitting saw, plunge not traverse cut which is what machined screws usually were before they went to cold headed slots.
@WinkysWorkshop4 жыл бұрын
Impressive! I'm glad I have two lathes, they have been handy on several occasions. I originally planned to sell one but can't bring myself to do it. The SB is more solid than by Logan but the Logan cuts slightly smoother and the carriage controls are easier to use.
@TomokosEnterprize2 жыл бұрын
@@WinkysWorkshop Decisions, decisions eh, LOL.
@WinkysWorkshop2 жыл бұрын
@@TomokosEnterprize The Logan is gone and I miss it now.
@TomokosEnterprize2 жыл бұрын
@@WinkysWorkshop I bet. We sure love our old iron eh.
@johncolvin2561 Жыл бұрын
You can avoid brass grabbing on a drill and pulling it into the cut by grinding a negative rake to the two cutting edges. That trick also works when drilling plastic.
@FestivejellyАй бұрын
I made a new cross slide leadscrew nut out of bearing bronze for my lathe. I ended up buying a 30cm bar and just chopped a section off it with a bandsaw. Then machined it on my 4 jaw. I then just used an M10 x1mm tap. It feels so much smoother than the stock brass one, and I know bearing bronze will wear a lot slower. Its worth spending a little time improving your lathes cheaper components, especially when they are easy to make.
@WinkysWorkshopАй бұрын
Bronze is better, how much is hard to say. The bronze use in bearings is usually not ideal (sintered) but some are solid. I haven't noticed any wear yet and my screw was near perfect.
@ronkellis7694 жыл бұрын
As always, nice job Winky. Glad to see the dial/handle didn't require fussing with like the Logan.
@WinkysWorkshop4 жыл бұрын
Thanks. I actually made an extension and made a larger dial. I need to put a self locking nut on the handle.
@ronkellis7694 жыл бұрын
I probably missed the video, and don't know anything about SB to have recognized a
@AmateurRedneckWorkshop4 жыл бұрын
Another Winky success. It is great when a plan comes together.
@WinkysWorkshop4 жыл бұрын
Thanks, yeah, it came together much better than expected. I figured the lead screw was worn.
@mshaw290808mi4 жыл бұрын
Thanks for inviting us into your shop .It was very enjoyable!
@WinkysWorkshop4 жыл бұрын
Thanks for coming
@OldtimeIronman4 жыл бұрын
Absolute genius! Believe it or not, I have actually used my lathe with both of the screws removed, takes a bit of planning but it can be done. Desperation and necessity breed interesting solutions.
@WinkysWorkshop4 жыл бұрын
Thanks!
@lawrencewillard6370 Жыл бұрын
Had backlash also. So, tapped thread in a 50mm block of propylene. Finished it off to fit, still had a little backlash. Heated it up a little, squeezed it in a vice, now tight. Cheap, easy and as I am 80, won't have problem again. Try it.
@WinkysWorkshop Жыл бұрын
Interesting... thanks
@lv_woodturner38994 жыл бұрын
Nice job. My SB Heavy 10 has a slotted shoulder screw similar to the one you made. This screw is flush with the cross slide. Odd that your SB had a proud screw. I can appreciate the frustration this caused you. Well done. Dave.
@WinkysWorkshop4 жыл бұрын
It is odd. South Bend changed there design after they made mine,
@dannywilsher41654 жыл бұрын
I fell asleep halfway through so I went back and watched it again. Nice job sir!!!!!
@WinkysWorkshop4 жыл бұрын
I'm not sure that was a positive of negative comment. I'm kidding, Thanks!
@dannywilsher41654 жыл бұрын
@@WinkysWorkshop LOL. I didn't think of it that way. I wasn't bored, I had just eat and you know a person can get a little sleepy after a big meal.... Hopefully they gave you two views !!!
@WinkysWorkshop4 жыл бұрын
@@dannywilsher4165 No worries... just messing with you.
@howardhughes63112 жыл бұрын
Nice job. I recommend that you drill a hole in a screw that you made and a small hole through the nut that you made so that you can oil that nut and you will get a lot more life out of it. That's the way it's done on a standard cross slide from south Bend.
@WinkysWorkshop2 жыл бұрын
That's a good idea. Fortunately the south bend cross slide cover comes off easy. I keep it well oiled. Thanks for the idea!
@rayfalcone68974 жыл бұрын
hello mr.Wink,another great job done by the master,i like it.......you wink i can not get over the way you get to the core of your work,its almost like deja vue....you and i work as if we were one person,all our conclusions end up the same.great video thanks for sharing,see you next time stay safe.
@WinkysWorkshop4 жыл бұрын
Thanks Ray, you're too kind!
@tedmattingly75644 жыл бұрын
Very nice fix, looks like it has been there from the start and made better than the original.
@WinkysWorkshop4 жыл бұрын
I think so too. Thanks!
@apollorobb4 жыл бұрын
If you want to take up all the backlash in the nut split the nut .250 in perpendicular from the back side and add a couple grub screws just cut it about 3/4 way through so when you tighten them it will spread the threads and take the lash out . Thats the way i did my old Clausing lathe and it worked great
@howardosborne86474 жыл бұрын
Same design as the adjustable leadscrew nut on my Harrison. The split line is about 1/3rd from the back side with 2 small Allen screws to do the adjusting of backlash with.
@WinkysWorkshop4 жыл бұрын
My nut was cast iron. It probably would not flex at all. My mill is made like what you describe.
@RAYAR543 жыл бұрын
Just subscribed. Great video. I just recently bought an 84-A (1928) this summer. Just had my cross slide apart a few nights ago and cleaned up the ways. Was checking out the cross slide nut and looking at replacing it sometime.
@WinkysWorkshop3 жыл бұрын
I like this lathe, was the bolt holding your nut sticking up ?
@RAYAR543 жыл бұрын
@@WinkysWorkshop Yes, it does have the bolt that restricts the rotation of the compound.
@WinkysWorkshop3 жыл бұрын
@@RAYAR54 Thanks, the only reason I asked is that after posting this video I had several tell me that mine was not original. I suspected it was and you just confirmed my suspicion.
@leehaelters61824 жыл бұрын
Love watching your process and the presentability of your workspace. Your narration also sounds a note with me, so you have my like and my sub without further ado! At 11:00, for brass and other soft metals it’s about the cutting edge, not the speed. Grind a wee bit of a land on that edge, at 90 degrees to the work, so that it takes a scraping cut. Of course, that dedicates your bit.
@WinkysWorkshop4 жыл бұрын
Thank you so much! Somebody else said the same about the cutting edge.
@ALSomthin Жыл бұрын
Lots of people making them. I did so as well a few years ago but made mine out of MDS infused nylon instead of brass. It is easy to machine and works great! This material has a lubrication factor built right in. It will outwear teflon in extreme conditions 100 to 1. Also you can drill a pilot hole all the way through a brass one, then drill a hole all the way through the bolt and use this to directly oil the screw.
@WinkysWorkshop Жыл бұрын
Yeah, I need to drill the hole for oil. I like the nylon idea but this nut is fairly thin, I'd be worried about strength.
@ALSomthin Жыл бұрын
@@WinkysWorkshop its not as strong as brass in compression but it is actually pretty rigid stuff. You should order a piece of it and check it out. I use it for lots of stuff I even put a piece of it on the edge of my old snow shovel for a wear edge.
@Morkmtw Жыл бұрын
@@ALSomthin I may try it but probably not for this lathe.
@kieranh20053 жыл бұрын
I built two nuts for the cross slide of my Boxford CUD lathe (improved copy of South Bend 9"). Mine were a composite, with a steel carrier and brass threaded insert (turned from some big brass bolts I scored for couple of coffees) I drilled the screw hole through until it was just breaking into the acme thread and tapped it. Then I stuffed half of a cigarette filter into the hole. I saw this on one of the machining forums. When I mounted the nut, before I put the grub screw in the top, I filled the hole up with oil. So my nut contains a wiper and an oil reservoir.
@WinkysWorkshop3 жыл бұрын
Thats a cool idea!
@davidmclean50674 жыл бұрын
Very nice! Unless they watched this video, very few would even know this was not a factory part.
@WinkysWorkshop4 жыл бұрын
Thanks... I got lucky, everything just worked!
@middleway1885 Жыл бұрын
I'd love to have seen these when I was a child... better late than never... Cheers!
@WinkysWorkshop Жыл бұрын
True, thanks
@georgebell71034 жыл бұрын
Nice video. My South Bend 13, 1978 vintage, is factory made pretty much like your modification.
@WinkysWorkshop4 жыл бұрын
I noticed that in some pictures - Thanks for the info.
@edwardkawecki81012 жыл бұрын
Same with my 1939 SB 11"×4'.
@MrJdorrington Жыл бұрын
Great project and well devised and explained. Many thanks.
@WinkysWorkshop Жыл бұрын
Thank you!
@shawnmrfixitlee64784 жыл бұрын
Great job ! That is a big improvement in my book , ENJOYED
@WinkysWorkshop4 жыл бұрын
I agree, Thanks!
@cleophusA4 жыл бұрын
I have a 1937 Pedestal style South Bend 11 inch and my cross slide isn't made like yours. Mine doesn't have the protruding bolt, but my lathe also has the taper attachment and I think that's the difference. It's nice to finally see someone else that has one of South Bend's "orphan" lathes!
@WinkysWorkshop4 жыл бұрын
I like the 11 inch lathe. Yes I was looking at a lot of pictures and most are made different. Mines a 1931.
@cleophusA4 жыл бұрын
@@WinkysWorkshop I could see that yours was older than mine from the apron controls, but many things do look identical. You wouldn't have an extra follower rest you're not using, would you? I have a steady rest, but no follower. Also, I am curious to see if your spindle threads are the same size as mine. Mine are 1 5/8 X 8 tpi.
@WinkysWorkshop4 жыл бұрын
@@cleophusA - Yes that's the size of my spindle too. I don't have a follow rest of steady rest although I plan on making both at some point.
@cleophusA4 жыл бұрын
@@WinkysWorkshop Oh, good! I'll look forward to seeing that. There's really only a couple of things I would like to get for my lathe that I don't have yet. One, as I said is a follower rest, and the other is a 3 or 4 jaw Buck or Bernard scrolling chuck. Do you have a supplier for cast iron backing plate blanks?
@WinkysWorkshop4 жыл бұрын
@@cleophusA - I prefer steel and make my own back plates. It's a big job but still worth while.
@richardtww4 жыл бұрын
Nice one , keep them coming always a joy to watch you making somthing usfull
@WinkysWorkshop4 жыл бұрын
Thanks Richard!
@elsdp-45604 жыл бұрын
THANK YOU...for sharing. Nice repair and fix. Watched and enjoyed.
@WinkysWorkshop4 жыл бұрын
Thanks! It went much smoother than I expected.
@iancraig19514 жыл бұрын
Winky a top fix with excellent video work..Really enjoyed it..greetings from OZ E
@WinkysWorkshop4 жыл бұрын
Glad you enjoyed it
@cdrive57576 ай бұрын
Hi Winky, I've done my share of tapping and also had my share of the dreaded broken tap when tapping small holes. I always use the accepted technique of backing out the tap a half to full turn often to help clear the swarf. I noticed that you also used this technique when you were tapping the Acme Cross Slide Nut. I mention this because I keep coming across KZbin posts that say never back an Acme Tap up or out. Since I'm going to be Acme tapping too I don't want to make any mistakes. I can say that looking how the Acme tap is tapered I can understand why it should be fed completely through the stock. Wakodahatchee Chris
@WinkysWorkshop6 ай бұрын
Interesting, I never heard this about the acme taps but it might be true. I've had good luck but it takes a lot of torque.
@cdrive57576 ай бұрын
@@WinkysWorkshop Funny, I was just watching, yet another Cross feed video and guess what he says? kzbin.info/www/bejne/fpO4q4KVesirn8U
@ianjones40712 жыл бұрын
Hi outstanding work love the mods, my son restored a 7 or 9 inch southbound, cheers mate
@WinkysWorkshop2 жыл бұрын
Thanks
@kentuckytrapper7803 жыл бұрын
Another job well done, I made one for my pratt&whitney lathe out of cast iron, that what the original was. Next time it will be brass.
@WinkysWorkshop3 жыл бұрын
Mine was cast also... I think brass wears about the same or a little better and it is easy to work with
@douglashank84803 жыл бұрын
I wonder if that protruding bolt head is the result of some previous owner's effort to "fix" a broken or missing part? I'm no expert at all on Southbend lathes, but I'd bet dollars to doughnuts that it left the factory looking a lot more like your 'modification' than it looked before you started. I simply can't believe that SB - or any other manufacturer of industrial machinery during that period - would produce a product with such a glaringly obvious (and easily avoided) design flaw. ...I have an 11" Logan (model 955) lathe that came to me with a couple of similarly bone-headed "repairs" that I've had to re-repair in ways that made more sense. Thank you sir for another excellent video! 👍
@WinkysWorkshop3 жыл бұрын
I don't know, it looked original but you are right... a silly thing to overlook. Thanks.
@nashguy2074 жыл бұрын
Great Job on the project. Fixed 2 problems at the same time!
@WinkysWorkshop4 жыл бұрын
Exactly! Thanks!
@MLCprojects Жыл бұрын
Detailed video that I will have to do soon too to remove my Cross Slide Backlash. Just a thought: with a countersunk hex screw instead of the shoulderbold less material would have been lost from the carriage?
@WinkysWorkshop Жыл бұрын
This seems like a good solution and it would have worked but the hole was fairly large from the original shoulder bolt. The material loss would probably be about the same but I was mostly worried about changing the location of the hole with the countersink.
@MLCprojects Жыл бұрын
@@WinkysWorkshop OK, lot's of good tips and ideas 😊
@WinkysWorkshop Жыл бұрын
@@MLCprojects It helped the backlash on mine a lot but it still has about .010 to .015
@TinhNguyen-mb7gx2 жыл бұрын
Great video. Great work. Thanks for sharing it. I have an old SB heavy 10 and I have the same issue. What’s the tap size for you used to tap fir the cross feed nut please? I’m an ammeter, I need all the help I can get. Thanks again
@WinkysWorkshop2 жыл бұрын
It was a 1/2"-10 LH Acme tap. I got it on ebay for about $24. I still have some backlash but it's much better.
@TinhNguyen-mb7gx2 жыл бұрын
Thank you for the information. I measured mine, it is a 7/16"-10 ACME LH thread. After watching your video, I disassembled mine and found a couple loose bolts that had contributed to the issue. I cleaned and reassembled the unit. I was surprised and glad that the backlash is much, much better now. .007” vs .018” of backlash. I wish I can completely eliminate it. What do you think about making an anti-backlash nut by using maybe one third of the old cross slide nut (I call it the tension nut) and bolting it to the new one with a spring in between them? In my case I would use a 1/2" dia X 3/4" spring outside the lead screw and two #10 bolts (in the area above it) to bolt the tension nut to the cross slide feed nut
@Morkmtw2 жыл бұрын
@@TinhNguyen-mb7gx - Honestly .007 is fantastic. Without ball screws and some kind of thrust bearing at the dial you can't expect much better than that. I think a anti-backlash nut of some type would help but I'm guessing you will always have .004" or more. I'm not sure it is worth the effort. I've seen people modify the nut by cutting part way through (as if you were separating the nut it into two nuts) and adding a small set screw that separates them at the cut. The uncut section flexes a little and removes the backlash when you tighten the set screw.
@howder19514 жыл бұрын
Nice job Wink, a little bluing and it will match the rest of those screws. Nice job on the brass, cheers!
@WinkysWorkshop4 жыл бұрын
Thanks you sir!
@MrCrankyface4 жыл бұрын
That's a beautiful modification, even looks stock!
@WinkysWorkshop4 жыл бұрын
Thanks, I'm glad it looks stock, I didn't milling my classic lathe but it added to it's function.
@ellieprice33963 жыл бұрын
Thanks for a well executed project that I also need to do on my Jet lathe. To prevent two flute drills from grabbing (self feeding) in copper, brass and bronze stone a small flat (.030) on each cutting edge to remove helix. How in the world do you keep your shop so clean? New sub.
@WinkysWorkshop3 жыл бұрын
I've heard that before... thanks!
@geoffmorgan60594 жыл бұрын
Good job! I notice your "other" lathe is a Logan. I had a Logan 10" for a long time, I liked it. I also had access to and used a South Bend Heavy 10. I really liked the SB taper attachment set up-it was like a larger lathe. I didn't care for the South Bend's spindle sleeve bearings. The machine was old, but the spindle didn't have excessive run out, the Logan just seemed to run smoother and cut easier.
@WinkysWorkshop4 жыл бұрын
I think my south bend if more solid but the logan cuts smoother. I like them both.
@cosprint Жыл бұрын
Great video. I have the same issue with the lead screw on my logan 10 inch, 820. We're did you get the tap for the lead screw nut? Also, how do I find the size of that tap. Should I just measure the lead screw and count the threads?
@WinkysWorkshop Жыл бұрын
The threads will always be 10 TPI if the compound moves 1/10" (.100") per turn. Some lathes do not but you 820 does. I'm fairly sure the Logan is 1/2" LH thread but you can measure the OD. You can get the taps on eBay or Amazon.
@cosprint Жыл бұрын
@Winky's Workshop Thank you for the reply. I just measured the thread and it's a 7/16 diameter. I will look up the tap on Amazon. Thanks for the help.
@WinkysWorkshop Жыл бұрын
@@cosprint No problem
@tomthumb30854 жыл бұрын
Top job. The factory should have done it this way as standard. Great video with none of the high speed footage, which can be annoying. Thanks.
@WinkysWorkshop4 жыл бұрын
Thanks 👍 I found out later that south bends changed there design later and made it the same as mine. I basically copied there design.
@nigelpearson29762 жыл бұрын
Where on earth did you get a left hand Acme tap (in 1/2"?). Not many machine shops would have one of those!
@WinkysWorkshop2 жыл бұрын
Apparently amazon has everything amzn.to/34tf4kQ
@clems69894 жыл бұрын
Curious why not use a flathead countersunk in the casting ?
@WinkysWorkshop4 жыл бұрын
A flat head screw would have worked although the shoulder bolt probably increased the strength a little. I basically copied the newer SB design.
@dannywilsher41653 жыл бұрын
I watched this again and didn't fall asleep this time!!!
@WinkysWorkshop3 жыл бұрын
Thanks Danny!
@bigbattenberg4 ай бұрын
Play/ backlash is inherent in any normal thread. With a conventional lathe, the play is always moved to one side so it's never a problem. CNC is a whole different ball game although the same principles apply. A really useful feature is a locking mechanism on any slide not in use for the operation at hand. If you don't have it invest time there. We have a Colchester Triumph 2000 lathe at work which I found has a very nicely executed locking mechanism for the compound, also the saddle can be locked. I have yet to locate the cross slide lock.
@WinkysWorkshop4 ай бұрын
Yeah, I should have titled the video, "Reducing backlash". You're right about a slide lock. I sometimes use a gib adjustment screw to do this but a separate lock would be great!
@bigbattenberg4 ай бұрын
@@WinkysWorkshop If you need tips on execution I could send some info on how Colchester did it - simple and effective.
@WinkysWorkshop4 ай бұрын
@@bigbattenberg I'm not sure if could be applied to my south bend but feel free to send pics. winkysworkshop@GMX.com THANKS
@bigbattenberg4 ай бұрын
@@WinkysWorkshop Hmm I just realized I will have to disassemble it again to take a picture. I'll look and see if we have a parts book at the shop or if I can find some image online.
@WinkysWorkshop4 ай бұрын
@@bigbattenberg Don't go to too much trouble.
@CraftedChannel4 жыл бұрын
Ok, A question. Did I miss you explaining the tap? I have been worried a standard Acme tap would have to much clearance and you'd end up with a lot of backlash. I've purchased a couple but not used them yet. You however ended up with good backlash which is encouraging. Did you use s special tight tolerance or standard tap?
@WinkysWorkshop4 жыл бұрын
No you didn't miss it. I thought I bought the tap on ebay but apparently I bought it on Amazon. Either way the G spec was not specified. I was actually kind of shocked that it was tight. This is the name of the tap if you need one. "MPI Tools Acme TAP High Speed Cobalt Steel 1/2" 10 TPI Left Hand Threads"
@bowlweevil41612 жыл бұрын
@@WinkysWorkshop I bought the same size tap on ebay for $13.70 to make crosslide nut for 1936 atlas 10d and had nearly no backlash! can't believe how well that cheap tap worked good vid thanx!
@WinkysWorkshop2 жыл бұрын
@@bowlweevil4161 Thanks! Yeah it worked great for me as well. I was worried about lead screw wear but apparently I didn't have much. Most of my remaining backlash is the adjustment near the dial. Thrust bearings would be a big plus.
@listerine-pr5lt4 жыл бұрын
Very good solution coming from an intelligent mind.
@WinkysWorkshop4 жыл бұрын
Wow... Thanks!
@BedsitBob4 жыл бұрын
Given the lead screw nut is keyed to the Cross-slide with the boss, did you really need a shoulder bolt? Wouldn't a standard Allen bolt have been sufficient?
@WinkysWorkshop4 жыл бұрын
You might be right although I just copied a more modern South Bend. Either way I'd have to counter bore and sink and the bolt was east to make.
@mftmachining4 жыл бұрын
That was a top-class job. Really good.
@WinkysWorkshop4 жыл бұрын
Thanks!
@jimbrideau58023 жыл бұрын
Good work. Extremely practical!
@WinkysWorkshop3 жыл бұрын
Thanks Jim
@countrycraftsman51103 жыл бұрын
Somehow i missed this video the first time. It seams like a right of passage when we start modifying our machinery to fit our needs. Another great build. Backlash is the bane of quality and by extesion ones sanity.
@WinkysWorkshop3 жыл бұрын
Thanks, Oddly enough, this modification made my lathe like most other South Bend lathes. Apparently this bolt was only used on early South Bend 11" lathes.
@mohabatkhanmalak11614 жыл бұрын
Very nice, usefull modification. Thanks for sharing.
@WinkysWorkshop4 жыл бұрын
My pleasure
@BedsitBob4 жыл бұрын
For internal threading, why not swing the compound in the opposite direction, so it is pointing toward the chuck, as seen from the operators view?
@WinkysWorkshop4 жыл бұрын
That is a option although it what you have in your chuck is large it will hit the back of the compound. You can lengthen the reach of the boring bar/ threading tool but that's not ideal. For me it is way easier from the back side. You hand is also clear of a moving chuck.
@alanray77744 жыл бұрын
I can't help but wonder if the bolt that caused the problem had been put there by a previous owner. My South bend has a recessed, slotted bolt very much like the one you made. On mine, however, the tapped hole does go completely through, and there's a small, drilled hole in the slot so oil can be applied to the nut.
@WinkysWorkshop4 жыл бұрын
I think they changed it shortly after 1931. I had to create a recess fr the shoulder bolt I made Without the recess there would be no way to make the bolt flush. Thanks for reminding me, I need to drill a oil hole.
@alanray77744 жыл бұрын
@@WinkysWorkshop I had forgotten that you had to mill out the recess...nice job. Like some others mentioned, that tap handle/guide should be my next project.
@WinkysWorkshop4 жыл бұрын
@@alanray7774 - Thanks Alan, you will love the tap handle. It's one of those easy useful projects!
@boostie10054 жыл бұрын
The Boxford Lathe, UK version of Southbend The Cross Slide Nut has a Long What you call an extension, it is fixed to the Cross Slide by a Grub Screw Which has a point Which pushes a small plunger in a hole @ 90deg to the "extension" . the extension is a good fit in the cross slide so no real movement of centreline.
@howardosborne86474 жыл бұрын
I was just going to mention the grub/pinch screw tightened onto the leadnut extension boss. It is a good method of securing the lead nut.
@JamesDedmon4 жыл бұрын
A creative fix for sure
@WinkysWorkshop4 жыл бұрын
Thanks James~!
@CraftedChannel4 жыл бұрын
Hard to tell it wasn't done that way stock. Which is a high compliment indeed. Very nice. It's silly how some try to keep their machines totally factory stock. Valuing a blue ribbon from a contest that does not exist. ;-)
@WinkysWorkshop4 жыл бұрын
Yeah... I like to make sure a modification is worthwhile before I alter a machine but if it's worthwhile I do it. Thanks for the compliment!
@raymondwoodring79774 жыл бұрын
Amazing job winky and.great job on the fix
@WinkysWorkshop4 жыл бұрын
Thank you !
@terrycannon5704 жыл бұрын
Could you please tell us what the ACME TPI and also where you sourced the Acme Tap
@WinkysWorkshop4 жыл бұрын
I got the tap on eBay. It's a LH 10 TPI x 1/2" Standard Acme. So far my all my lathes have used this size in the tail stock and cross slide.... the compound might be 3/8" but I'm not sure.
@terrycannon5704 жыл бұрын
@@WinkysWorkshop Thanks for the quick response. I need to do the same on both of my clausing lathes. I found a guy that sells the Southbend nuts but i will need them for my Clausings. If the tap is priced reasonable i may just buy the tap and make them myself. Again thanks for the reply and the video.
@WinkysWorkshop4 жыл бұрын
@@terrycannon570 No problem, thanks for watching
@shanek65824 жыл бұрын
Winky's Workshop will that same thread size fit a 10” atlas craftsman lathe? (made in 1942) thanks
@WinkysWorkshop4 жыл бұрын
@@shanek6582 - I think so but you need to measure the OD. It will be 10 TPI but it might be 3/8".
@TheKnacklersWorkshop4 жыл бұрын
Hi Winky, Nice job there... Well done... Will you be making a screwdriver for the extra wide slot next - lol Take care Paul,,
@WinkysWorkshop4 жыл бұрын
Thanks Paul, nah, the regular large screw driver works fine.
@MrModify2 жыл бұрын
Nice job. I need to do this also. How did that brass nut hold up?
@WinkysWorkshop2 жыл бұрын
It's holding up very well. Most the backlash is at the dial. Ideally a set of thrust bearings would be helpful but space is an issue
@anthonycash46094 жыл бұрын
I bought a cross slide brass nut for my south bend a while back off eBay that was made to fit a South Ben for the same reason , I was hoping it would cure my backlash problems , most everyone I asked about it said it would due to the nut was brass and the screw was steel and the nut would ware out first. It helped but I still have quite a bit of backlash and not sure what to do at this point.
@ronkellis7694 жыл бұрын
Take a look at the handle/dial. Not knowing exactly what you have I can't look at a parts diagram, but the Logan lathes depend on adjusting the inner nut as tight as possible while retaining free rotation then tightening the handle to the inner nut. I use a very thin bicycle hub cone nut wrench to hold the inner nut.
@WinkysWorkshop4 жыл бұрын
Mine is near perfect now which really surprised me. My original nut was cast iron. I think what back lash I have left is from the adjusting nut like Ron Kellis said in his comment. You have to have some backlash. I have 3 or 4 at most. I was planning on replacing the lead screw if necessary. I was going to cut the screw off and bore the gear and braze a new one in place. Glad I didn;t need to do that.
@anthonycash46094 жыл бұрын
@@ronkellis769 thanks for the info , I will take another look at it.
@anthonycash46094 жыл бұрын
@@WinkysWorkshop winky I took mine apart today and was able to adjust it like Ron said and get it much better. On mine the handle you turn is put on with a 12\24 thread and a small split nut that holds it tight. I guess in the past life of it someone has worked on that before and the small threads that hold the handle is nearly nothing left. 2 threads at most. Have any clue where I could buy a cross slide screw for it. It's a 9 inch south bend. I also could not get the dial to come off either removed set screw also. Didn't won't to chance messing it up more and not having one to replace it with. So put it all back together. It's better but don't trust the little screw and nut that holds the handle on now.
@WinkysWorkshop4 жыл бұрын
@@anthonycash4609 Let me get back with you tomorrow. I took mine all apart and modified it with a new dial. I remember having a terrible time getting a handle off but i think that was the compound. In the mean time watch this part of my video. kzbin.info/www/bejne/a4C9dK1qpN6ibsU
@Tensquaremetreworkshop4 жыл бұрын
Really love that tap handle! My next project...
@WinkysWorkshop4 жыл бұрын
Yes the tap handle is simple and super nice. Thank!
@fpreston95274 жыл бұрын
You made that look easy. And neat
@WinkysWorkshop4 жыл бұрын
Thanks... I'll admit, it went smoother than expected.
@mats7023 жыл бұрын
Nice work man, enjoyed the video.
@WinkysWorkshop3 жыл бұрын
Thanks !
@kerrywil14 ай бұрын
I made my cross slide nut with bronze and a $20 left hand acme tape from EBay. I made 2 with a spring in between the nuts. I can send pictures?
@WinkysWorkshop4 ай бұрын
Bronze is better.
@WinkysWorkshop4 ай бұрын
I think bronze is better
@dannywilsher41654 жыл бұрын
OH boy, a new video from Winky!!! Now I will watch it...
@WinkysWorkshop4 жыл бұрын
Hello Danny! thanks for watching!
@ottostasi82263 жыл бұрын
Nice job , what kind of drill press do you have ? Nice to have that auto up & down travel .
@WinkysWorkshop3 жыл бұрын
The drill press is a Dayton. It's not the greatest but it has two features i like. 1) a 6-inch quill travel and 2) a split casting at the quill. As for the motor drive, that's a harbor freight drill... VERY handy. The round column has been replaced with a square which keep everything aligned when you move the table plus a made an x y table. kzbin.info/www/bejne/n2XCd6eDgrKZetk
@Bassman733 жыл бұрын
Hi, i noticed you've used a parting blade for normal turning, is that recommended? Or is that some special tool that i'm not aware of? Thanks for the video.
@WinkysWorkshop3 жыл бұрын
It's called a grooving tool. You can part with it but it also cuts side to side. They are great for cutting a square shoulder.
@kentuckytrapper7804 жыл бұрын
Great video wink' I need one for my pratt&whitney lathe 5/8 8tpi. Don't have the skills yet to make my own. Wered you get a left hand acme tap?
@markthompson48854 жыл бұрын
I have a Pratt & Whitney lath too. a model M1689.
@kentuckytrapper7804 жыл бұрын
@@markthompson4885 were is the model # located?
@WinkysWorkshop4 жыл бұрын
I got it on eBay... $22 I think.
@alexvonbosse50904 жыл бұрын
Nice job! Thanks for sharing and keep up your great work!
@WinkysWorkshop4 жыл бұрын
Thanks for the visit
@kallibrand41064 жыл бұрын
A job well done !!! I have to do the same on my lathe pretty soon since the backlash in the cross slide is now becoming a real pain . I will have to cut the threads on the nut on the lathe though . Thank you for sharing this .
@WinkysWorkshop4 жыл бұрын
This old Tony did a video where he tapped inside acme threads. The tap is way easier and only cost me $22 on ebay. Thanks!
@chrisschoeny67343 жыл бұрын
why did you choose to use brass instead of steal? I need to do the same repair on my Montgomery Ward (Logan) lathe
@WinkysWorkshop3 жыл бұрын
Brass wears a better than steel although bronze would have been ideal but the main reason was that it was very easy to machine. Using an Acme tap in steel is doable but very slow going.
@lwoodt14 жыл бұрын
Where there's a will, there's a way. Nice job.
@WinkysWorkshop4 жыл бұрын
Thanks
@leehaelters61824 жыл бұрын
Great project, nicely done! Taking out the backlash is a great result. I don’t see why you had to hide the top of the bolt, though. Is it because the compound would not swing even 120 degrees? How did Southbend never realize that folks would be threading things internally?
@WinkysWorkshop4 жыл бұрын
I've looked at all kinds of pictures of south bends and they all have a recessed bolt. Apparently they corrected this on later models.
@mradtke664 жыл бұрын
Not being able to swing a compound 360 degrees is odd, but you don't need to swing it so far to thread internally. For normal, right hand threads cut by moving the tool toward the check, swing the compound 30 degrees to the right. Advance the tool with right hand turns of the crank, pushing it into the work (I know you know how to do this, just setting the stage for step 2.) For internal, right hand threads, swing the compound 30 degrees to the left. Advance the tool with left hand turns of the crank, "pulling" it into the work. As an added bonus, it keeps all of the controls on the front of the apron. Reaching over the ways to dial in a cut for threading seems silly to me.
@Engineerd3d4 жыл бұрын
Excellent work. Enjoyed it.
@WinkysWorkshop4 жыл бұрын
Thank you sir
@kerrywil13 жыл бұрын
thanks for the video great job. time to buy a broaching tool for the lathe
@WinkysWorkshop3 жыл бұрын
Thanks
@philipdenner8504 Жыл бұрын
Well done that man.
@WinkysWorkshop Жыл бұрын
Thank You!
@grahameblankley38134 жыл бұрын
Very well planned out, now looks as though it's always been like that.
@WinkysWorkshop4 жыл бұрын
Thanks, yes and that is a good thing. I hated to drill the casting but the original design was limiting.
@daveticehurst41914 жыл бұрын
Winky, you really did not need to make a new shoulder bolt, as the nut was now located inside the original 1/2 " hole in the cross slide. All that was needed was to retain the nut from dropping out when you removed the cross slide in the future. You could have just countersunk the cross slide 1/2 " hole and fitted a standard countersunk Allen screw or even just a slotted soft screw. The Manufactures only used a shoulder bolt to take the load on the nut, you now have no load on the new nut as it is now located in the 1/2" hole. Tip for drilling brass / Perspex ect. to stop the drill grabbing, is to "back off" the cutting edge with a few rubs with an oilstone. This is to make the drill a NEGATIVE rake tool. As an accomplished woodturner, you should know this with your negative rake scraper, and found out that a standard tool will grab. Another great project and video under your belt, well done. Thought, should you want to reduce the backlash you have, make a thin nut say 1/4 inch thick and fit a compression spring in between it and the original nut. That will keep a tension between the leadscrew and the nut at all times. You may need to add a tiny anti rotation pin between the original nut and the "washer nut" otherwise it could rotate slightly and jam in the saddle. If you have a 3 d printer, you can see the idea on the Z axis . Stay Safe and Well.
@WinkysWorkshop4 жыл бұрын
I thought about that too. I should have made a longer extension on the nut. Still I feel a little better with the steel thread going into the brass and nut. There is a lot of force on the brass, if nothing else I think it would get loose over time. Also the way I did this is just like the later model South Bend lathes. I wonder if lower RPM would have helped the drill and the mill grabbing. I'd hate to blut the edge of my drill for one hole.
@stefantrethan3 жыл бұрын
Do you think the internal thread on the leadscrew nut could be turned on the lathe? I can't find the right taps for mine.
@WinkysWorkshop3 жыл бұрын
I think so but Acme threads are much harder to cut than standard. You'd probably have the grind a tool to fit inside the nut. What size do you need? I've never had a problem finding a tap.
@WinkysWorkshop3 жыл бұрын
Randy Richard did this kzbin.info/www/bejne/iaa5onyYjamohNE
@stefantrethan3 жыл бұрын
@@WinkysWorkshop Thanks, that looks like something I can handle. It's a metric nut 18x5mm, while 18x4mm is the common pitch. I even found a tap, but it is right handed and I need left.
@WinkysWorkshop3 жыл бұрын
Here's one on ebay www.ebay.com/itm/174946576041?hash=item28bba0e6a9:g:JTsAAOSwl6Rf8rW7
@stefantrethan3 жыл бұрын
@@WinkysWorkshop Thanks, that is most useful. For some reason I forgot to check in China.
@andyZ3500s4 жыл бұрын
Nice fix on the new nut Winky. You have to like going from. .040 play to under .005 play. The modification that you did on the cross slide looks like it came from the factory that way, especially with the flat slotted bolt. It is hard to believe that it was originally designed where you couldn't cut a ID tread.
@WinkysWorkshop4 жыл бұрын
Well you can cut thread with the compound to the left front but the chuck tends to get in the way. It looks like South bend corrected this problem after my lathe. Mine if a 31 model and a guy commented that is 1937 lathe was not made like mind. Thanks for the comment Andy.
@tonypike57854 жыл бұрын
Thanks for the show, great job
@WinkysWorkshop4 жыл бұрын
Thanks for watching!
@michaelmounts12692 жыл бұрын
Great video...was the tap an acme 8tpi???
@WinkysWorkshop2 жыл бұрын
It was LH 10 TPI. It has to be 10 for the dials to work right.
@michaelmounts12692 жыл бұрын
@@WinkysWorkshop Thanks...you've inspired me to tackle the same issue on my Log n 10"!
@WinkysWorkshop2 жыл бұрын
@@michaelmounts1269 Great. I think it might be a little easier too.
@mootan2 Жыл бұрын
great work as always.
@WinkysWorkshop Жыл бұрын
Thanks
@waynep3434 жыл бұрын
Think of this. Use a tap Drill to drill 2 holes across above the acme thread on either side of the 3/8-16. Counter bore the holes for button head Allen's. Use tiny belville springs or high compression rate springs only 1/4" or 5/16" tall. Cut an angled slot from the top beside the stub sticking up into the upper acme hole. Now by varying the button head tension you can vary the grip on the cross slide screw automatically. You may end up boring a little out of the acme hole to allow it to contract on the acme thread angle instead of bottoming out in the root on the screw. It's just a thought depending on how worn your lead screw is. You could also slip some wick felt into the slot to oil the lead screw. Drill and shallow tap a hole in you cross slide for an removable set screw to oil the felt once In a while. Again. Only a thought.
@WinkysWorkshop4 жыл бұрын
Thanks for the input. I'm not sure there is enough room to do this although I might try if the nut starts to wear. Currently the amount of backlash is very slight and even slightly tight on one end of the travel. Also, when I ran the tap through the nut again it opened a small hole between the mounting bolt threads and the acme. I think I might drill a small oil port in the mounting bolt.
@waynep3434 жыл бұрын
@@WinkysWorkshop if you drill a hole thru the mounting bolt.. put a piece of felt at the bottom of the 3/8-16 hole in the brass part..
@WinkysWorkshop4 жыл бұрын
@@waynep343 - Sounds like a plan.
@dannyh82884 жыл бұрын
Where did you get the proper left hand tap with whitworth(?) threads for the brass nut?
@leehaelters61824 жыл бұрын
Danny, surely they are Acme threads, no? All the supply catalogues have left hand threading taps, I am quite sure. In the USA, try McMaster-Carr, or MSC.
@WinkysWorkshop4 жыл бұрын
Yes it was a standard acme. The nut fit perfect.
@WinkysWorkshop4 жыл бұрын
Oh... 22 buck on ebay.
@gvet474 жыл бұрын
⭐⭐⭐⭐⭐ You earned five stars! Nice work.
@WinkysWorkshop4 жыл бұрын
Yay! Thank you!
@danhoag3734 жыл бұрын
did you buy or make the tap? if so how much and where?
@WinkysWorkshop4 жыл бұрын
It's a LH 1/2" x 10 TPI tap I bought on ebay for $22. Amazon also has then for about $35.
@houdini96973 жыл бұрын
how do you oil your cross feed nut and shaft?
@WinkysWorkshop3 жыл бұрын
I just give the threaded rod a shot of oil. Several have suggested drilling the top of the screw... probably a good idea.