You're the best, dude. Not only did you pioneer this inventive swap, you stand behind your work. Really appreciate you, can't wait to feel the car at full power.
@tturi28 ай бұрын
should feel supercharged now 😅
@BETTALIFE1018 ай бұрын
He has to. Everything by is on social network now.
@bigk138 ай бұрын
All right Ben, no excuses now 😅. Can't wait to see what the 2024 season has in store for you guys.
@BETTALIFE1018 ай бұрын
@@bigk13 it’s a Toyota still. Still won’t be the Honda.
@mattfransen41318 ай бұрын
2grfe swap when
@roberthowse27538 ай бұрын
Love to see the failure mode identified, proven, and so well explained! Awesome vid!
@fastinradfordable8 ай бұрын
And not spoiler’d❤ Thanks Robert
@mawwalmazie8 ай бұрын
Running that lean would've been catastrophic and yet he pushed it round the track until it finishes, it's a miracle that cylinder survives. Great to see comprehensive diagnostic Marc, thx for the vid.
@FrankensteinMotorworks8 ай бұрын
Unfortunately there was no sign of running lean, i was even there at the mid-ohio loss to look at logs and try to figure out what was going on and even I told him that despite being down on power everything was running right so to keep taking it out there. From what i understand the injector was going from running to fully shutting off quick enough that the engine never spent much time in the running lean region of operation so nothing burned up.
@mawwalmazie8 ай бұрын
@nsteinMotorworks So it's the works of a faulty injector that made those behavior then? In your vid it seems that the 4th injector are almost fully absent on high frequency (rpms), I think it might've behaved differently like you said it being shutting off briefly when they're connected to the ECU, since all the sensors can detect abnormality from the engine.
@kenny2408 ай бұрын
@@FrankensteinMotorworkscould it have also been a situation where the other 3 cylinders were running rich, offsetting the lean condition of the #4 (as far as the readings on the WBO2 is concerned)? Was duty cycle checked in the logs to see if the duty cycle of the injectors was abnormally high?
@FrankensteinMotorworks8 ай бұрын
@@kenny240Yes, the abnormal fuel use did show in the logs but we were seeing airflow inconsistencies also so there was a bunch of stuff that together did not align to a diagnosis. In hind sight it's very obvious with the information i had but i did not put it together at the time.
@kenny2408 ай бұрын
@@FrankensteinMotorworksI know how that goes. It happens in my line of work all of the time. Nobody is immune to it. It’s still a win though.
@oregonfelder18 ай бұрын
The deductive methodology you used was probably the best possible way to diagnose this issue. Each step kind of was necessary in order to rule out everything else.
@mhtate36268 ай бұрын
I strongly agree. I realize it's easy to say this with hindsight AND from the peanut gallery but with those injector test results I'd immediately be wondering "Did I burn up valves?" , "Is there scoring in that cylinder now?" etc.; I wouldn't be able to sleep without confirming the rest. Sucks doing an engine pull to just to find out the real problem but at least it removes uncertainty down the road.
@ryanbrown57278 ай бұрын
Been missing you Marc! Good to see a new upload buddy!
@FrankensteinMotorworks8 ай бұрын
Sorry about the long time off, I do have good plans for 2024 so hopefully it'll be a good year.
@ryanbrown57278 ай бұрын
@@FrankensteinMotorworks No worries man! Looking forward to it!
@stinkbra8 ай бұрын
"whole motor for something that would take 10 minutes to swap"... It DID also make a very, very cool video for anybody that follows you and G&G
@DaMurphMurph8 ай бұрын
No longer own my 2011 tC but I still will religiously watch your content. Keep up the great work you’re doing Marc!
@FrankensteinMotorworks8 ай бұрын
Careful, if you watch long enough you may end up wanting another car with a 2AR or 2GR :) Thanks for sticking around
@DaMurphMurph8 ай бұрын
@@FrankensteinMotorworks I wouldn’t mind that 😉 I have a 2018 WRX as of now. I just ported and polished the factory turbo and installed billet turbo wheels. Currently making around 340whp, but it’s nowhere near as reliable as my Scion was. The car had almost 200K on it and needed some work done to it, mainly just suspension components and drivetrain mounts due to them being old and almost all original. My ideal build was forged internals, with your cams and valve springs, and a turbo. I just couldn’t justify spending that much money on all of those performance mods and ignoring what actually needed to be fixed on it. My Fiancée owns a 2016 tC with a 6-Speed, so I still get my fix tC when I’m driving her car. Love the fact she wanted it to be a 6-Speed since she learned how to drive manual in my car.
@ricecakeFTW8 ай бұрын
That injector test was insane!!! 😮
@38tech8 ай бұрын
Bro!!! But literally a man of the scientific method. Not everyone does that.
@3ormorecharicters8 ай бұрын
Wake up! There's a new FMW video up.
@TheCordrick8 ай бұрын
Yes sir yes sir
@thecliff8028 ай бұрын
I cant explain exactly why but your videos have this style to them that makes it seem like a really amazing lecture AND entertaining. Like I feel like I am more calm and more intelligent and more relaxed after watching this
@waseembux75378 ай бұрын
Marc is a legit genius LOL. We need him here in South Africa. Guy needs to create an academy or something.
@bigk138 ай бұрын
Way to go Marc! I met you and the Ben's at Mid-Ohio and we actually discussed the lack of power that day on the tracks dyno..... Full circle and here we are with an answer to the riddle. You are a wizard and this video put a huge smile on my face knowing this weight is off your shoulders now. Hope to see you all again at Mid-Ohio this coming season 🤘🤘
@shaunh2278 ай бұрын
Nothing will teach you more than seeing a master solve a new problem. Really interesting and honest video… and some closure!
@alpinevicemotorsports18058 ай бұрын
Very happy to see it fixed. I bet it feels good to have that mystery solved. I hope Ben has an opportunity to enjoy the car this year
@tedmich8 ай бұрын
Ouch! Rich is a bummer but lean is a killer, good that you figured it out! I had a I4 Camry and an injector died, at very high RPM is felt almost normal.
@speedacademydave8 ай бұрын
Nice detective work, and thanks for sharing the whole process so openly. Really interesting to see your process. Have you guys considered throwing some ID injectors in that bad boy? They do an amazing job of balancing and characterizing their injectors.
@FrankensteinMotorworks8 ай бұрын
Injector dynamics really does make some nice injectors and what they do is crucial when you larger flow injectors but the goal of showing off this build was to show off what could be done with low budget using only factory parts. Keep in mind this motor is build using OEM toyota hybrid 2AR-FXE camshafts. I have other builds on my channel making much better power that do use Bosch 980cc injectors but when i grow beyond those i will likely be contacting injector dynamics for bigger ones.
@TheYakkis8 ай бұрын
Most of the population is asleep now while I'm leaned in and locked onto every piece of information. Lol. I hate that you had to do a full tear down but sometimes it's gotta be that way. Fascinating . Thank you
@ReignitedAuto8 ай бұрын
Holy cow what a weird failure! No surprise that so many people looked at it and couldn't find the issue. I have a couple weird ones like this every year. Always a pull your hair out scenario until you finally find the source. Congratulations on persevering and finding the root cause! 👏
@Irishtwincam7 ай бұрын
Well done Marc. Nice to have closure on what the issue was!!
@johnmann7o26 ай бұрын
Marc, I think developing the 1ar has more potential due to more displacement and could potentially beat the k24. As of now, this scion motor doesn’t even have variable valve timing, just a k24 minus vtec.
@senatorchinchilla53898 ай бұрын
Cool to see such detailed diagnostic work.
@Shift-happens-tv8 ай бұрын
FUCK YEAH BUD THIS DAY CANT GET FUCKING BETTER NEW FUCKING VIDEO FROM MARC LETS FUCKINGGGG GOOOOOOOO
@stevebarnette8 ай бұрын
Boosted Boiz had problem like this a few years ago. Glad you figured it out. Looking forward to seeing the car go faster in the future.
@neillgarcia58 ай бұрын
Your such a wizard.. genuine dude.. still replies the little ppl's questions... and doing big things with ⚙️&⛽️... dope stuff..
@josuelopezcarrasco79338 ай бұрын
Im mindblown to see how you figured out the problem. Good stuff Marc!
@Stephen_Ellis8 ай бұрын
This encouraged me to go check my fuel injectors, and get them flow tested.
@FrankensteinMotorworks8 ай бұрын
i certainly know i will be doing it more often now. Especially since i have the machine right here
@thedmango2358 ай бұрын
this dedication and transparency deserve a follow, thumbs up. loved the explanation!
@FrankensteinMotorworks8 ай бұрын
I really debated if i should post this at all, i expected the internet to call me an idiot for not noticing this earlier but the responses have been surprisingly positive. But no matter what i try to be as honest as possible with my results on these engines so even failures have to be shown and everyone can learn something.
@josephmatuszak38558 ай бұрын
Would love to see Ben have a successful season coming up!
@11metalfan8 ай бұрын
Love seeing someone put the hand up and stand behind their work, and also admit when they're stumped with something Funnily enough, the best way to show competence and knowledge is by admitting you don't know something. Straight away you can trust the guy that knows enough to say he doesn't know
@Elmanret8 ай бұрын
That is what a real mechanic does, you are amazing!
@AlexTrull8 ай бұрын
Great to see an honest look at an issue like this. Full respect.
@LHT-Casual8 ай бұрын
That's such a wild finding, sucks that you had to tear down the engine before you found it. Love seeing this saga come to an end, now it's just up to how well Ben can handle his schizophrenic chassis on the track! Looking forward to this season for sure @GearsandGasoline!
@Wirenfeldt19908 ай бұрын
Awesome sleuthing boss! Now you know that this is a thing, so a full tear down should not be needed.. Live, learn and document.. Can’t wait to see Lin get on track again
@mhtate36268 ай бұрын
Awesome work paired with great explanation. A silver lining, among many others is that at least there wasn't catastrophic component failure.
@FrankensteinMotorworks8 ай бұрын
Yeah, i am very happy that the motor was actually still in great shape. That part honestly really surprised me. I would have expected a melted down cylinder with this kind of failure.
@Colin-s5b8 ай бұрын
you are the best and most responsible mechanic I have seen on youtube
@finboyYYC8 ай бұрын
Glad to see more content!
@Treacherous_One8 ай бұрын
I figured it was something simple. glad to see its solved.
@FrankensteinMotorworks8 ай бұрын
Yeah, it really was truly small and simple but i'll be damned at how hard this thing was to find. It was not a fun hunt.
@Treacherous_One8 ай бұрын
@@FrankensteinMotorworks BUT, you have a new thing to look for when doing a preliminary evaluation moving forward. so it wasn't really time wasted as it can save you from repeating this in the future.
@CollinWalther8 ай бұрын
Awesome video! Great story telling, and thank you so much for not making me wait for a second or fifth video for the conclusion!!!!
@FrankensteinMotorworks8 ай бұрын
I'm glad you enjoyed it and yeah i really don't like keeping people on the hook for a conclusion.
@patrickfowler46738 ай бұрын
Good luck to Ben Lin and his Mr. Two. I'm glad you figured it out. Good to see content from you and Gears and Gasoline.
@chase2768 ай бұрын
Cars are simultaneously the best and worst thing ever. I’ve never had something make me feel as angry and also happy as fixing what i thought was a complicated issue on my car that turned out to be a simple fix.
@vinnycent0078 ай бұрын
I have been watching/following you for two years now and love seeing the progression on the 2AR-FE and its variants. As an Engineer myself, I love your though process and execution as it was well planned out. I currently own a M/T 2014 scion tC for 4 years now and I was thinking of AWD converting the car. I have been looking at the rav4 AWD as a donor parts as the architecture is similar. The problem I would see is the parasitic loses in the drive train, but looking at your simple modification to increase the HP really could make this project work. I love to see what future innovations we will see this year for the engine.
@FrankensteinMotorworks8 ай бұрын
Usually the biggest issue with an AWD conversion is getting a big enough trans tunnel and still having space for the fuel tank. the 2014 tC also has the EB60 transmission and that has no center differential option so if you go AWD you'll need an electronically controlled clutched rear differential or switch the transmission for the previous version that does have a center differential option available.
@christophercasale79618 ай бұрын
What about an EAWD conversion with the rear unit from a Highlander?
@zev40368 ай бұрын
Great video! Super thankful to have you pioneering the 2ar communities road to power! Can’t wait for the stock ecu cams 👍
@donoursizemore96868 ай бұрын
Holy crap Marc! I just got off the dyno with a 2gr that was behaving eerily similar to this unexplained fuel trim asychrony (> 10%), missing power but not a whole cylinder work. I had been searching for a spark problem, but none exists.
@FrankensteinMotorworks8 ай бұрын
Hopefully sharing this does end up helping someone. Thankfully getting injectors tested is relatively simple.
@pv40838 ай бұрын
Toyota reliability + this genius is a good combo
@Dylanbforthree8 ай бұрын
This was such a cool breakdown, loved seeing your thought process through the diagnosis.
@vertigo91na8 ай бұрын
Thank you for posting and sharing your knowledge. Great insight into what actually happened and solid reminder to always check the basics first.
@ice9dragon8 ай бұрын
I love the way you explain things, you're a genius👌
@craig71118 ай бұрын
What a nightmare to troubleshoot! Well done!
@WarriorsPhoto8 ай бұрын
Seeing that it was an injector was good. Here's why? We can learn from others to stick to the simple things first.
@FrankensteinMotorworks8 ай бұрын
Yes, perhaps this video ends up saving someone else a bunch of headaches.
@WarriorsPhoto8 ай бұрын
@@FrankensteinMotorworks Amen 🙏 to that. Appreciate your humble share.
@timwise68768 ай бұрын
Grest to see this video Marc, thanks again for you help recently, cheers from Aus, Tim & Jamie 2GR 😆
@ravynx8 ай бұрын
Nicely done, Marc. Love to see diagnostic videos like this.
@SurferSandman8 ай бұрын
Wow that was really interesting. Thanks for the troubleshooting thought process, very interesting.
@Karsten-cc5ws8 ай бұрын
Wow, after 8 months a new video! Can only hope that it doesn't take that long for the next one. :)
@candycornpeeps8 ай бұрын
Great explanation as always. Please keep posting. I love your thoughtful explanation of things.
@GOTTHEFUZZ8 ай бұрын
I'm not sure if the Haltech that you guys are using has the capability, but it probably wouldn't be a bad idea to start using EGT sensors on all the build proceeding this one. It really helps with diagnosing this type of problem.
@jeffman38 ай бұрын
Always glad to see another upload. This one must've been a bit more than mildly upsetting.... A full teardown to find a faulty injector. Woof.
@Genevagirls-h2x8 ай бұрын
Glad to see you sorted this out man!!! You are an amazing mechanic and i always look forward to the uploads!!!! Also VERY hyped to see the spyder back on the grid to its full potential!
@FrankensteinMotorworks8 ай бұрын
Thanks for watching the video, i appreciate it. I hope to have some interesting content out in 2024
@tolkienleung8 ай бұрын
Been following this, thank you for the complete explanation. In the very early beginning of understanding EFI and standalone tuning, i went through two different sets of injectors that one of the 4 went bad. Not easy to pinpoint without experience and the right tools. Individual egt sensors would be nice but not all can afford to.
@kovacspis8 ай бұрын
You posted a new video so soon after my "where'dyougo" comment on your previous video hah. :D Welcome back, it was a great episode with great content of a nice car. (I watched the video within 5 minutes of you publishing it but forgot to comment until now)
@FrankensteinMotorworks8 ай бұрын
Thanks for sticking around while i took a break. Content should be a bit more regular for the rest of 2024
@martron78 ай бұрын
It's good to see the little red mr2 back in shape ❤
@FrankensteinMotorworks8 ай бұрын
Yeah, i can't wait to see how he does with the car now that it has the power it was supposed to have in the first place. It's still at a bit of a disadvantage for the GLTC class but 15% more power should still make a big difference.
@martron78 ай бұрын
@@FrankensteinMotorworks I've got a silver MR2 third gen pre-facelift with a hardtop, So, this project has a special place in my heart.
@KanzakiXL8 ай бұрын
Hell, I’m gonna push my Camry 2AR to at least 230WHP, I just wish those camshafts weren’t out of stock.
@dillankennedy96078 ай бұрын
i was commenting to check the injectors from the begining.
@FrankensteinMotorworks8 ай бұрын
and it appears you were correct. The issue is i've never seen an injector fail in this manner before and also by the time the videos are posted we had been debugging this for months already.
@baddoges8 ай бұрын
MY EJ motor @ roughly 12:1 compression on E85 was giving me 230psi in each cylinder. Except the one I blew the ringland on.
@FrankensteinMotorworks8 ай бұрын
turbo motors tend to have much shorter duration cams with much less overlap so those numbers will be quite a bit higher.
@e51419818 ай бұрын
welcome back glad to see you back at this, cant wait to see what the future holds
@FrankensteinMotorworks8 ай бұрын
Thanks for being patient, i promise it won't be so long before the next one :)
@IanMarshall-i1m8 ай бұрын
Good to see you back. Always informative and helpful material. Best wishes.
@Jacky1Feng8 ай бұрын
Deep dive figuring out issues, fantastic content
@Cb7sohc8 ай бұрын
Great vid, a lot of work went into this
@derekyam18058 ай бұрын
These failures are the ones that really rip your hair out and take years off your lives. Glad you stayed in it and figured out the problem, bet that felt like you discovered Atlantis lol
@nolo24848 ай бұрын
What an odd failure, luckily it didnt burn a valve! Great video
@FrankensteinMotorworks8 ай бұрын
Yeah, i'm honestly surprised it did not cause further damage.
@danielcgomez8 ай бұрын
All I can say is ...there's a first time for every type of failure/fault! ...Great job finding the fault!
@stirch98 ай бұрын
Yay. Glad to see you making more content! I want a 2AR in my MK1 MR2.
@stirch98 ай бұрын
Steps for checking injectors. Remove engine and disassemble head......... Double edge sword with this one. It was only the injector. But you had to take the engine apart. But luckily it wasn't something catastrophic.
@FrankensteinMotorworks8 ай бұрын
Yeah, i took the really really long way around on this one. But to be fair many other professionals had taken a look at the car and not figured it out either so i don't feel that bad. Just slightly annoyed i had to do that much labor to figure it out.
@nissan20028 ай бұрын
Marc love your technical knowledge 👏 keep this content up
@thunderlighting20068 ай бұрын
Wow theres always something that throws off even the pros so interesting to learn about tho
@andrewroland84918 ай бұрын
Reminds me of back in the day. first step to find the problem is measure the individual header pipes temps. A little more wild with carbs tho
@jonathanmatthew54518 ай бұрын
Awesome breakdown of the issue and fix! Great content
@erikmiles55368 ай бұрын
Had a similar but less dramatic issue with my 1ZZFE and injectors that were out of balance. Did some fun things to the 2 different banked fuel trims.
@Jose_44618 ай бұрын
I’m 5000 miles into my 2gr swap and I love it I’d like to do a aw11 2ar at some point i just love your work 🤙🏽
@nehok8 ай бұрын
Great to see you got to the bottom of it! Even if it did take you more disassembly than you would have liked.
@FrankensteinMotorworks8 ай бұрын
Yeah, dropping a motor twice, once to carefully check that the motor is still in time and another for a full disassembly just to find a bad injector certainly was a bit more than i was hoping for.
@420basco8 ай бұрын
thats such a weird problem, cant wait to see the results this season
@dangreenwood67558 ай бұрын
Very interesting video, really enjoyed the content and the way you presented it!
@ian_ford8 ай бұрын
Something similar happened to me. I developed a sudden idle issue and notice my oil (on the dipstick) was milky. I disassembled the motor (not the short block) and discovered the head gasket was fine. I spotted a horizontal line of oil residue on the turbo cold side after disassembly. The side of the turbo that faced the valve cover. It never occurred to me the idle issue was that the seal for the valve cover was blowing air and oil. Air was getting in past the VC seal. In part because I had switched to a 2 into 1 catch can system (crank case vent and VC vent), and it was overwhelming it. So, had I kept my old 2 catch can system that worked, I wouldn’t have had higher pressures in the head…and I wound’t have had the valve cover gasket failure, which caused the idle issue. 🤦♂️ Cost me labor, a new head gasket, new VC gasket and other ancillaries. 8/10 times, the issue is simpler than we think.
@flambo99508 ай бұрын
I knew my goat would pull through
@reneneron29718 ай бұрын
Glad to see you back, Marc. Hindsight is always 20/20, and the tune wasn’t the only problem. Simply amazed that the engine didn’t burn up on cylinder number 4 running that lean (saved by running e85?). I am still baffled why this wouldn’t show up on fuel trims, as the ECU would add STFT to compensate for the lean condition on #4…which would also reduce power on the remaining cylinders as a result of being rich. The reversion to the “base” tune, which pulled ignition timing, may have what saved the engine during Ben’s race. E85 (which lowers combustion temperatures and tolerates more ignition timing) and the less advanced ignition timing from the wrong base tune likely prevented a catastrophic failure.
@FrankensteinMotorworks8 ай бұрын
It did actually show up on fuel trims. We figured that out a while back but we could never figure out what that positive fuel trim meant. in hind sight we certainly should have dug further into those positive fuel trims. I think the biggest thing that saved the engine was that the cylinder almost entirely shut down, it was probably well below the low flamability limits at higher RPM. But that's not the entire picture since we do have evidence on the valve that it was running hot when it was running.
@reneneron29718 ай бұрын
@@FrankensteinMotorworks it likely shut down at wide open throttle and close to redline, but if it was idling acceptably and dropping flow at higher injector duration, it had to run lean in between idle and full throttle. The good news is that no damage was done. I don’t think it would have worked out that way on gasoline, though I am speculating.
@FrankensteinMotorworks8 ай бұрын
@@reneneron2971I can say that it was fine on gasoline. several of the outings it did have pump gas in there.
@reneneron29718 ай бұрын
@@FrankensteinMotorworks with the retarded ignition timing though, yes? You are likely right…under high load conditions, it likely was too lean in cylinder #4 to he combusting at all.
@ricepony338 ай бұрын
I recently had an entire set of injectors fail, took a long time to figure out the issue!
@OhOmah8 ай бұрын
omg Marc from Frankenstein Motorworks, I'm your number 1 fan
@PajamaSenpai8 ай бұрын
Can't wait to see this back on the track!
@FrankensteinMotorworks8 ай бұрын
Me too, Ben is a great driver and i want to see this thing putting some decent times down.
@kowalskitk48 ай бұрын
great story. thanks for sharing.
@garage79r8 ай бұрын
Last few years Its become a regimen for anything I am working on to have the injectors checked and cleaned. Recenty had a rb26 come in for some service work with some mild driveability issues. Turns out 2 injectors were not as strong as the rest.
@FrankensteinMotorworks8 ай бұрын
I've had other issues with injectors, that's why i bought that machine to begin with. This did not give me those indications but you're absolutely right, i think injectors will start getting tested just as a matter of course these days.
@garage79r8 ай бұрын
@FrankensteinMotorworks yeah it does not take long and saves future headaches
@kumakaroshi1178 ай бұрын
Awesome work, thank you.
@drumjedi53018 ай бұрын
Now THAT is digging in and finding the issue. Killer stuff, man. Question: would a 2AR swap make sense in an AW11 MR2? A 220ish hp NA engine in that car would make for an awesome daily/back road burner...
@dannoyes44938 ай бұрын
Frankenstein is ALIVE ! Well Done.
@trutaing8 ай бұрын
Awesome work! Interested to this motor in rwd format!
@nicholaskallmyer98658 ай бұрын
Been waiting on this video for a while. Thank you!!
@aplong19118 ай бұрын
Well done!!! Great videos thanks for sharing!👍🏼😊
@billyquist92378 ай бұрын
Awesome job Marc 👍
@gabzor47168 ай бұрын
Congrats on finding that problem, love your content, I wish you crossed to the dark side with K-swaps for MRS just cause your support is so much better haha
@FrankensteinMotorworks8 ай бұрын
There's just not enough hours in the day, there are already two other Toyota engines i really want to explore so there's no time to spend on the K. I also feel the 2AR is a superior motor but i get that this isn't always the way people make their decisions.
@jrbuch8 ай бұрын
I once had a set of 550cc injectors on my 1JZ VVTI that weren't firing properly. The car never ran right.. even when tuned. It just didn't make the power it was supposed to. It was only AFTER i'd upgraded to a set of 1000cc injectors and increased my power goals, and sold the set of 550's, did I find out what was wrong with them (when a mate who bought them, told me he had to get them cleaned, flow tested and that they were uneven.
@nathanchildress55968 ай бұрын
I’ve got an AW11 MR2 sitting in my yard with its stock 4AGE on a stand. Knowing that engine is the same price and makes double the power has me in a real pickle.