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ProMod Randy Boosted SBF has MAJOR issue! What do you think happened?

  Рет қаралды 10,585

Turbo John

Turbo John

2 ай бұрын

Well, we got more problems than we had in mind. Let's work through the process to see if we have a minor problem or a major problem. Sometimes, as you work through the tear down you start figuring out what happened and why it happened. Stopping and taking the time to pull the pan liekly saved Randy a very catastrophic engine failure. We still have some failures, but no broken rods that would have surely come at some point soon........ What do you think happened? Follow along and we will show you!
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Пікірлер: 94
@24sharpy24
@24sharpy24 2 ай бұрын
John, would be cool to see the datalogs to show the difference and what you found in the oil pressure.
@boostedgringo5885
@boostedgringo5885 2 ай бұрын
Please don’t mess around with that rod bolt being difficult. I’ve trashed a block, rod piston and crank trying to keep the rod with an imperfect threading.
@barrywright1311
@barrywright1311 2 ай бұрын
How Randy keeps a smile is beyond me! He’s a laid back guy but damn all I see is dollar signs and I’d be a mess lol
@robertbray5735
@robertbray5735 2 ай бұрын
Can’t wait till it’s fixed……dam I looking forward to see ya at Orangeburg…….take care..
@onealmason5046
@onealmason5046 2 ай бұрын
Tough luck fellas...glad y'all caught it when you did tho 👏💪💪
@jorginofingal4267
@jorginofingal4267 2 ай бұрын
Keep going Randy and John
@mooklocklear1182
@mooklocklear1182 2 ай бұрын
Man, I hate to see that, hopefully this next refresh will solve all the issues
@baby-sharkgto4902
@baby-sharkgto4902 2 ай бұрын
When it rains it pours, damnit. All part of it
@jtcoker2684
@jtcoker2684 2 ай бұрын
Dang man that sucks. Although, it’s a damn good thing y’all decided to do preventative maintenance!! That would have been bad if not. Myself, I can afford preventative parts but when it ruins the whole motor, that’s when it hurts the ole sphincter!! Y’all will get her going again no doubt
@jamiecrider2513
@jamiecrider2513 2 ай бұрын
Don't get discouraged Randy, it's awesome that you guys caught all of this when you did. Could have been a disaster! Keep chipping away and stay positive.... I love TJ's attitude and approach to the sport.... Life is great with friends working on their racecars ... Building memories and doing what you love. Hang in there fellas, praying for you guys...
@ScottSmith-dd6iy
@ScottSmith-dd6iy 2 ай бұрын
Piston contact will normally be valve guide wear and side loading the valve over to the piston. Just open up the piston or back cut the valve a tiny bit. and put new guides in it, probably valve guide wear. check rocker arm geometry too. I have seen it get into the cylinder walls . run a reamer thru the bolt holes to open the bolt clearance a little. Good luck.
@philbetthauser9547
@philbetthauser9547 2 ай бұрын
It's terrible to see that happen but fortunate that you caught it before a major blow up. .
@robertdouglas3456
@robertdouglas3456 2 ай бұрын
Regular maintenance is a great thing to do especially with a 3000 horse power Ford 427 motor! Great job TJohn & Randy!🤩🤩
@jonsetzer9556
@jonsetzer9556 2 ай бұрын
Piston rock is causing the valves to hit. The skirts on the pistons are bending in causing more rock.
@young11984
@young11984 2 ай бұрын
Thats why its made to be easy to work on, better to pull while in one piece than in many pieces
@keysautorepair6038
@keysautorepair6038 2 ай бұрын
That’s crazy maintenance omg it gets to a point where it’s just not worth it anymore.
@DSRE535
@DSRE535 2 ай бұрын
That’s racing especially when you’re pushing the limits of the parts!!
@joshuagibson2520
@joshuagibson2520 2 ай бұрын
Dont chase those threads John. A tap cuts and makes chips. Use a thread foormer aka roll tap. It forms the thread and pushes the material back where it needs to go and doesn't remove material.
@tomhamilton9140
@tomhamilton9140 2 ай бұрын
Hope you get the problem fixed soon and can get back to racing.
@freddiemoralez1536
@freddiemoralez1536 2 ай бұрын
🎉🎉❤ YES 💯 2810 hp IS A LOT OF POWER. THANK GOD THE ISSUES WERE FOUND BEFORE 🎉🎉🎉🎉🎉 thanks for the update
@docsmallblock6584
@docsmallblock6584 2 ай бұрын
Dang that's a bummer! Randy has spent more money on that engine than I could ever dream of yet has had nothing but problems with it! Should just buy one of those new GM 632's and be done with that Ford junk!
@young11984
@young11984 2 ай бұрын
My opinion, when the thrust bearing wears to where all the load is on the front roller thrust then the crank may be flexing at that journal vs the thrust containing that flex. May want to countersink the head bolt holes so it doesnt squeeze the aluminum in on the studs
@xxkingslayemxxgamer5553
@xxkingslayemxxgamer5553 2 ай бұрын
The engine builder should have caught the valve Clarence issue before assembly
@dewaynelong7198
@dewaynelong7198 2 ай бұрын
With great power " yall caught alot before it became worse..FoMo4thawin
@electrochubb
@electrochubb 2 ай бұрын
*I find it mind blowing that motor was making ~3000 hp with intake valves hittin'.....what the hay.?*
@Blain5700
@Blain5700 2 ай бұрын
PMR saw TJ blow up his SB and said, "Hold my beer..." Letssss Gooooooooo!!
@mitchdenner9743
@mitchdenner9743 2 ай бұрын
Well, gravity feed off that tank wouldn't work with no vent, and that's the catch can's job so if the line has oil sitting in it its not vented. Plumbing 101 air behind water. Adding a vent to to the tank will defeat the catch can and make a mess so looks like you'll have to straighten that hose out.
@davidreed6070
@davidreed6070 2 ай бұрын
Take it out. Sadly. Ive been waiting for you guys to get the bad boy stuck and cranked up.
@jaygullion8013
@jaygullion8013 2 ай бұрын
Tough luck fellas! You get it right again you always do! BTW was that your new mustang behind you TJ
@Lucky_Nemo
@Lucky_Nemo 2 ай бұрын
Not a car guy but us bike guys will have valve reliefs on the "meat" of the crown on the pistons to get the valve reliefs
@ysitrim88
@ysitrim88 2 ай бұрын
Hmmm seems to me the whole block is flexing! I just don't know how strong that aluminum block is??? Also how much did you guys allow for the aluminum rod stretch? That engine is milliseconds from total destruction! Time for a billet block. Good luck.
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
Head gasket thickness.
@jerrypennell544
@jerrypennell544 2 ай бұрын
Ok Big John, at pump 1 needs to be the Sump, 2,3 to the pan
@jamiemuncy2219
@jamiemuncy2219 2 ай бұрын
I run a 9.5 in Windsor based Man O War Iron block and I'm 468ci I've had almost all the problems yall are having in the past all but the roller cam bearing problem. Must be where mines iron and not aluminum, ide say heats an issue. I run a roller thrust only on my crank too. My problem is I beat the skirts up pretty bad between seasons. Don't know why but I always have the same two pistons beat up lol
@HeadFlowInc
@HeadFlowInc 2 ай бұрын
I vote “Fat n Sassy” add a little more bearing clearance to give it more cushion before contact plus added cooling of the oil etc. 👍
@billjenkins1416
@billjenkins1416 2 ай бұрын
You need the inserts for the head stud holes machined and pressed in, that is an annoying problem.
@lukk4273
@lukk4273 2 ай бұрын
Wonder if pistons hitting the valves would cause the knock sensor to go haywire too if they run one.
@auriceburrell8148
@auriceburrell8148 2 ай бұрын
Hardest thing is your running classes that you have to be the fastest so you have to push the limit every run. It's not a 4000hp engine and only using 3000hp, your running it at max everytime
@garylucier6817
@garylucier6817 2 ай бұрын
Sad, I would go crazy. Too few passes- too many $$$$%%.
@skiphardstuff7444
@skiphardstuff7444 2 ай бұрын
Almost any machinist and or decent engine builder would known and fixed that off set . And if yall can't tell THE PINION ANGLE IS WAY OFF for optimum performance has too be associated with ANGLE that is constantly variable, however it has to be NEGATIVE ANGLE INTENTIONAL Initially till up ON LEVEL FOR LEVERAGE . BUT I DONT KNOW ANYTHING. DO YO THANG...
@Hjfvvdst
@Hjfvvdst 2 ай бұрын
So the converter is pushing the crank too far? Seems the converter needs more room or an issue with the converter is causing an engine issue. I think Steve Morris had this issue. He checked the converter clearance found it didn't have enough room. I don't remember how much room from the flex plate it needed. I also think I remember the converter drove itself into the Trans pump and damaged it. I think the fix was a spacer in-between the engine and bell housing.
@jkfonyi
@jkfonyi 2 ай бұрын
Speaking of Jason Tyson where is he ? Also why have a roller thrust if you’re still using the internal thrust ?
@jamesdavis4859
@jamesdavis4859 2 ай бұрын
What up bro
@danieljones685
@danieljones685 2 ай бұрын
Looks like the pin needs to be clocked a degree in the piston
@garylucier6817
@garylucier6817 2 ай бұрын
That is a ton of glitter.
@realazliving
@realazliving 2 ай бұрын
I think it needs a bigger turbo. 😮
@nashguy207
@nashguy207 2 ай бұрын
Poor Courtney you never cut him a break or give him any slack. I probably wouldn't either. 😆😆😆
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
We have great conversations for sure... I just am recording it most times when I'm dishing it out.....lol
@RustyWells2
@RustyWells2 2 ай бұрын
Randy had about of enough he's going to go Big Block!
@turboman351w3
@turboman351w3 2 ай бұрын
only 14 passes and it spins a main bearing, something is very wrong somewhereTKM WILL DEFINITLEY FIX IT
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
I'm thinking the thrust wore, and grabbed the bearing. Once it turned, then there was no oil getting to the bearing.
@bradleyslusser2279
@bradleyslusser2279 2 ай бұрын
Poor Randy .
@davidreed6070
@davidreed6070 2 ай бұрын
You guys ever file the thrust so it and the front share the load.?
@BrettBennett-nd5vd
@BrettBennett-nd5vd 2 ай бұрын
CAN YOU PUT 2 BEARINGS BACK IN IT THAT HAS THE GROOVE ON THE TOP AND BOTTOM?
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
I don't know, would not probably hurt anything to get extra oil
@garylucier6817
@garylucier6817 2 ай бұрын
That is a bunch of issues.
@BFTEgodswarrio5939
@BFTEgodswarrio5939 2 ай бұрын
Main reason mustang guys use ls engines over ford motors. Friend told me years ago 302/5.0 engines are good street engines. But not very good drag car engines unless you are running 351w block or a bbf.
@royrichardson9164
@royrichardson9164 2 ай бұрын
This is a engine that made over 2800hp on the hub. It doesn't matter if it's a gm, ford or chrysler at that hp level it's gonna always have problems because almost every part is aftermarket
@thesquirrelchroniclesakare7808
@thesquirrelchroniclesakare7808 2 ай бұрын
The question is WHY did it spin the main ?
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
I think the thrust gave up first.... then that maybe grabbed the bearing and turned it that robbed all the oil supply
@thesquirrelchroniclesakare7808
@thesquirrelchroniclesakare7808 2 ай бұрын
@@TurboJohnRacing I think you caught it just in time
@jasonhastings5538
@jasonhastings5538 2 ай бұрын
How is Jason?? Is he doing better after the wreck??
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
Yes, he is good. Went to the track a few weeks back with the old Hulk car with his driveline. Said it was fast
@jasonhastings5538
@jasonhastings5538 2 ай бұрын
@@TurboJohnRacing right on!!!! Glad he is back racing!!!!
@88_turbo_fox73
@88_turbo_fox73 2 ай бұрын
Wow that sucks, so much money in that motor for it to just not last
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
It does, but it's racing. The fast, fast guys put rods/pistons in 10-15 passes, new cranks 50 passes. And those are the very best of the best parts.
@royrichardson9164
@royrichardson9164 2 ай бұрын
How long you think a 3000hp engine last?
@jeffgraham48
@jeffgraham48 2 ай бұрын
Race car!!! Constantly....
@rcracechannel1636
@rcracechannel1636 2 ай бұрын
Just a thought but if the crank is/was bent could that cause contact with the valve?
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
Maybe, but it appears straight
@rcracechannel1636
@rcracechannel1636 2 ай бұрын
@@TurboJohnRacing I’ll be looking for an update on it. I grew up drag racing in the nineties and have a little knowledge of how an engine works and I enjoy your videos. Hopefully I will get to an event and meet y’all. I even though I grew up in a Chevy family, I love Randy’s car it’s beautiful. That red almost looks like torch red, the same color we used on our cars. Oh yeah another reason my mind went to the crank was because of the thrush bearing. Thanks for the reply and I can’t wait to see your new car.
@garylucier6817
@garylucier6817 2 ай бұрын
That will beat the hell out of a thrust bearing when the valves hit the pistons. What was the thickness of the head gaskets?
@garylucier6817
@garylucier6817 2 ай бұрын
Remove every valve, spin each in a lathe, you will find many of those are bent. Just my 2 cents, all those hitting pistons will be bent slightly.
@garylucier6817
@garylucier6817 2 ай бұрын
John, did TKM assemble that short block? And was piston to valve clearance checked during assembly?
@garylucier6817
@garylucier6817 2 ай бұрын
All the damages can be tracked back to a single issue. All that valve contact w/pistons. Now, to find out if it originates with heads, pistons, or bent crank...that is like a really tough one. Valve angles to piston valve reliefs, head gasket thickness, rod stretch, crank straightness? What a freaking nightmare to determine. Even pushrod length and spring binding. Something more than a small thing.
@lukk4273
@lukk4273 2 ай бұрын
Also wonder if maybe there was some valve float causing the valves to hit the pistons.
@supertunesupertune
@supertunesupertune 2 ай бұрын
@@lukk4273 That statement is true for the exhaust valves... as the piston chases the exhaust valve when closing, but the Intake valve chases the piston, so even if it does float, no chance of it hitting the valve relief .
@user-nf2ht5ku7b
@user-nf2ht5ku7b 2 ай бұрын
Damn it’s broke more than it’s not
@ecaldrone
@ecaldrone 2 ай бұрын
piston is probably rocking and hitting the valve when the engine is cold; less cold revving, less P2W clearance, smaller intake valve, or less lift.....the lifter bushings need to thicker and have more of an interference fit....same with the cam roller bearings, or locate them with snap rings or thrust blocks......rely more on the roller thrust, that's what it is for....(I am not a machinist, just some dumbass commenter on KZbin).
@justincurry2907
@justincurry2907 2 ай бұрын
Should go big block or coyote
@FoolPullDiesel
@FoolPullDiesel 2 ай бұрын
C only a real tuna catch something like that!
@derrickbasenberg811
@derrickbasenberg811 2 ай бұрын
What definitely happened was he still hasn't hired a pro tuner
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
Because “Pro” tuners don’t blow shit up? 😂 Go sub to Steve Morris channel, or go watch some of the NPK KZbin channels. Or just go to the track and walk the pits and see what’s happening on the high horsepower cars. Shit breaks all the time!!!! Tune didn’t kill this one, rod bearings good, plugs ok, piston tops not melted! Not saying I ain’t killed engines from tune up, because I have. Just like the pros!!!! Tell me what killed this one? Specifically!!!!!
@user-mm1se7gy7e
@user-mm1se7gy7e 2 ай бұрын
What do i think ? . . . . CHEVY TIME !
@erikalston4496
@erikalston4496 2 ай бұрын
Randy get an Oberg 😐
@JohnClutch1
@JohnClutch1 2 ай бұрын
I hate to like videos like this but it is what it is. Late nights grow hair on your chest.
@TurboJohnRacing
@TurboJohnRacing 2 ай бұрын
I've had a lot of late nights, lol
@JohnClutch1
@JohnClutch1 2 ай бұрын
That oil pressure EKG saved the motor!
@JohnClutch1
@JohnClutch1 2 ай бұрын
Good luck with the new car coming! Can't wait to see what you can do with a few extra cubes.
@noonecareswhenalltheydo
@noonecareswhenalltheydo 2 ай бұрын
tell him to put a real engine in that thing!! LOL
@stevemayo1175
@stevemayo1175 2 ай бұрын
So Here is a Mouth full of Worthless Information ! When you Put it Up On the Trans Brake and the Stutter as Ignition is Interrupted on random Cyl's the Converter is Moving IN and OUT of the front Pump ever so Slightly that it is causing this to Happen ? this is only a Guess and Courtney you keep the Maverick at Home we don't need another Broke Race car take it to a Car Show / / Solution If the Front Bearing Can Keep the Thrust In Spec then Yes Cut the Sides Off the Middle Thrust bearing and Just Let Her Rip Good Luck Guy's
@Stevesbe
@Stevesbe 2 ай бұрын
⏲️ ⏳️ for TKM
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