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@jimshort65762 жыл бұрын
19:45 Jimmy's fatherly concern for Ant is what makes Jimmy such a stand up man. The little things I notice bout each of you lmao. All amazing people stay safe out there and warm.
@Joe_kickass252 жыл бұрын
@@CANDY-in9js Can a carrot fix are boy Jimmy’s issue?
@Joe_kickass252 жыл бұрын
@Lucifer Sorry i don't speak Egg roll
@leeshah68602 жыл бұрын
Boost Creep......Port wastegate in exhaust housing to encourage the gases to go through the gate rather than straight through the turbine 👍
@benw16202 жыл бұрын
+1, I remember skid factory doing this on chinese turbos, looks like the same issue here.
@isaacshively67052 жыл бұрын
Or get rid of the shitty internal waste gate and get a quality external waste gate... Or say fuck it and turn up the boost cut
@givman20042 жыл бұрын
Same thoughts. Even with the gate open the turbo can spool up and make boost on the inlet side. Either increase the gate size or control the boost on the intake side with a blow off valve.
@isaacshively67052 жыл бұрын
Or get rid of the shitty internal waste gate and get a quality external waste gate... Or say fuck it and turn up the boost cut
@isaacshively67052 жыл бұрын
@@givman2004 no blow off valves!
@leonrixon57862 жыл бұрын
Check to make sure the actual physical flapper on the gate is moving when open. Then you can rule out the turbo being the issue, plenty of people here in Aus have turbo na sr’s and have no issues with the stock ignition. But also doesn’t mean that yours is good! Just do smart coils and make sure the flapper is opening.
@helplmchoking2 жыл бұрын
Yeah was gonna say, you guys in Aus and us here in NZ are pretty experienced with DE+T motors, SR or RB! Others have mentioned porting the manifold to get rid of the stepped bit which can help. Otherwise it might be external gate time which is kinda a pain but not too bad
@wobblysauce2 жыл бұрын
Yep, nothing wrong with a little port job, some are really bad and others only need a little trim.
@tspans14082 жыл бұрын
Had the same issue on my sr20det, I was hitting 15+ on a 6lbs internal gate. Ported the wastegate hole but that only kept it down 1-2 psi. Swapping to external gate was the only thing that fixed my issue. But if you got a bigger turbo exhaust housing laying around the shop that might help also before going external. SR IS GOOD!
@tylerakerfeldt72202 жыл бұрын
SR IS GOOD is the message an auto enthusiast cult leader would spread to gain followers
@Broyourenglishisgood2 жыл бұрын
Jimmy got Brian back with the 2 step 😂 Donnie almost dying from Brian’s 2step from his mk2 is still my favorite Clip of all time
@ashaik69472 жыл бұрын
Anyone buy yugioh cards from jimmy shops and they come with random merch? I think it’s pretty cool
@thatoneguyclayton96212 жыл бұрын
Got my DBZ card and some wild 90s junk air fresheners.
@scaldeddogengineeringcolle70042 жыл бұрын
I bought that shirt for Bhalls build and it came with a card LOL
@aldenrichie2 жыл бұрын
I bought bhalls shirt and some stickers and didn't get a card. I was actually looking forward to seeing what random card I got ha
@baltazard133T2 жыл бұрын
Here's the thing with high compression engines and small frame turbos. The higher compression forces so much air through the exhaust manifold that the simple internal wastegate with its small dimensions cannot keep up no matter what. If you notice all of the big bad ass cars that are high compression running small or medium turbos have multiple external waste Gates on the system in the highest flowing areas of their exhaust manifolds. Some even have to go to the extreme of putting a wastegate on each exhaust runner just to manage their boost when they're compression is high. The trick for running a high compression engine with a turbo is to use a larger turbo, the larger turbo will negate the low end torque that destroys the engines and will stop the boost spiking as it will allow the boost to come in later in the RPM more controllable.
@wobblysauce2 жыл бұрын
Yep, compression isn't the killer for boost. Could go for big singles but most do multiple smaller so you have better control over the flow, just take a little bit of work to put them in/if you have space for it.
@closewatermelon2 жыл бұрын
Plot twist, What Jimmy thinks is open is actually closed
@bmbgarage34052 жыл бұрын
Lmao I actually researched the turbo to see if this was the case. Stock turbo shows wastegate arm point down from exhaust inlet
@NicoSchrauwen2 жыл бұрын
Thanks for showing this Jimbo, actually learned a lot about turbos today.
@NoClassic2 жыл бұрын
I wonder if the flapper is getting stuck or is loose on the arm? Is the initial downpipe elbow at all restricting the gate flow? Also not a bad idea to replace the distributor cap and rotor.
@paulsensabaugh78792 жыл бұрын
Turbo elbow is likely restricting waste gate flow. Needs a divorced turbo elbow.
@TabMcLain2 жыл бұрын
I think most wastegate actuators are welded on and then held on with a circlip at the flapper inside the manifold. As unlikely as it could be, I still had the same thought - maybe the flapper inside the manifold is just not opening all the way (or at all). Could be clogged with carbon? Or as I commented below, on rx7 turbos the wastegate port is just too small from factory, so it needs porting.
@iamapathy37802 жыл бұрын
we had a similar issue with a celica Gt4, but in the end it was the distributor cap
@bmbgarage34052 жыл бұрын
I just looked at a past video and the isr elbow he used has an oval pipe to the flange to accommodate the wastegate. Interesting detail though is that he never shows the elbow being off of the turbo so it's hard to determine what it's like inside.
@bmbgarage34052 жыл бұрын
I also had the thought that maybe he had a rag or paper tower in an exhaust port that got sucked into the wastegate vs getting shredded in the turbine. It's a stretch at best but maybe haha
@DaltonBalkwill2 жыл бұрын
Brian looking stylish today with those glasses 🤘🏻😂
@strictlylyrics_2 жыл бұрын
Watching old Jimmy videos boom Jimmy uploads great moment🤌🏽
@paulsensabaugh78792 жыл бұрын
Try a divorced turbo elbow. It has a piece to keep the exhaust gasses from over powering the waste gate gasses. Had to do the same on a KA with a GT2876.
@matthewstrine2 жыл бұрын
Agreed
@ryane58852 жыл бұрын
Id pull off the downpipe and see the wastegate move. I had t25 turbo do 15psi on a fwd b15 sr20 using the oem wastegate with a manual boost controller. It’s still alive.
@nickbrooks51362 жыл бұрын
The lever that connect to the flap is broken so it’s staying closed the whole time. Hence building all the boost no matter what position you try. Hope that helps and keep up the good works guys. Killer videos!!! A cool obs Chevy regular cab short box build with a turbo LS would be sick to see and something a little different you can put your twist on.
@802Garage2 жыл бұрын
According to some sources I can find, the rods and pistons are actually the same. The head combustion chamber is what makes the compression ratio different. The bottom end can generally handle quite a bit, but obviously you have to avoid knock.
@beastoftheeast21462 жыл бұрын
Brian looks like he is about to perform rocket man for you in the shop
@Odd_Redneck2 жыл бұрын
ok this is goin to drive me bonkers. the ramps for the dyno, square stock steel across the end of the ramps and a perunamtic bottle jack lifting on the bar thus lifting the ramps. 12 ton at napa. go get it. square u bolts are at O'Reilly on the sales floor. 🙃 that air filter is asking for trouble.
@hpmikereed59942 жыл бұрын
Ant has progressed soo much with his confidence on camera that he has highkey became more entertaining as a person 😂💯
@chrisdines13912 жыл бұрын
Has the wastegate seized shut and the lever broken off so it moves ? That’s the only thing I can think of
@W5ZMB2 жыл бұрын
This was my thought
@fredrikandersson38852 жыл бұрын
they tried 2 wastegates tho
@chrisdines13912 жыл бұрын
@@fredrikandersson3885 they tried the actuator, not the wastegate itself. The wastegate is built into the turbo
@flaviogoncalves55942 жыл бұрын
There talking about lever connected to opening valve at manifold
@bubbalove50972 жыл бұрын
First thing I thought of. Need to see the thing moving to make sure it isn't cracked and stuck mostly closed.
@TalkTime42 жыл бұрын
I always put the wastegate on the exhaust housing, 44-60mm gates never had boost creep like this, but yes higher compression is def enough on a 4cylinder, they want to breathe so you got to give them bugger manifolds downpipes etc for them not to want to boost creep
@ItsJoshN2 жыл бұрын
I love these videos/builds. Its probably boring to some but its a great experience to follow along and learn and read the comments and see everyone working together to figure out the issue.
@Triplenickelmotorsports2 жыл бұрын
going thru this with my son's turbo L28 Datsun... the hole behind the wastegate flapper was too small to relieve boost, we tried running it with the gate rigged open and it was still hitting boost cut. We are machining out the gate opening before we go to a turbosmart actuator
@bobsagit102 жыл бұрын
Donny with the goofiest line of all time I love it 😂😂
@magnetic03142 жыл бұрын
For future reference, exhaust restriction will reduce boost creep. It's common on a lot of 2J based cars to install a restrictor flange in the mid pipe to control boost creep. Less flow= turbo can't spin as fast= less boost
@paulsensabaugh78792 жыл бұрын
Had to do the same on a 2.2l eco tech with high compression and a small turbo.
@gimmethecarkeys2 жыл бұрын
Jimmy. Theory is actually backwards on the backpressure issue. If you exhaust was restricted your boost would be lower. Like having a clogged cat. I had the same issue on mine. We were trying to target 28psi on my car and would only hit 17 and was super lazy. Found out cat was failed. Ended up gutting the cat and then we turned the gate duty down and hit 36psi and was overboosting and having creep issues. You need to port the inside of the hotside where the flapper is.
@ArneFinstad2 жыл бұрын
There's already been comments about it, but this is a major issue on small turbos with IWG's! Port the wastegate hole and get a bigger flap, then it will be OK or you can go external gate, but then do a oversized one, that's how you controll small turbos on high comp and high displacement engines
@joshuapaquette22452 жыл бұрын
Pull the turbo, and port the internal wastegate to match the valve seat. If you see any pressure drops, change the back housing.
@bhhamblin2 жыл бұрын
Sometimes the port in the housing for the wastegate flap is too small and causes boost creep/ spike. Porting open that hole may help with flow.
@MrAudi2202 жыл бұрын
could it be the cam overlap, i know N\A engines have a overlap intake/exhaust so that the gasses flow better which is not needed on turbo engines since the turbo is creating enough flow, so in theory if there is too much overlap on this srDE it means that it blows boost into the exhaust which keeps the turbo boosting since it is exhaust driven,could be wrong and it could be something else but just helping to brainstorm here.Hope this helps👍✌️👉
@draggonhedd2 жыл бұрын
Jimmy pull off the turbo and check the actual wastegate hole under the flap. They can be EXTREMELY too small for the size of the turbo sometimes and you need to drill em out/port them so they can actually flow enough when the gate is open. Theres a reason why people dont use internal gates anymore.
@Mike.0982 жыл бұрын
2 things. Timing ok from crank and cams? And check if the turbo gate internaly is ok. I hade a guy that had mounted it wrong. When actuated it closes instead of opening. The waist gate was working backwards.
@Jayco9x192 жыл бұрын
I can never miss a jimmy oaks upload😮💨
@nismonolo2 жыл бұрын
fun to watch you try & diagnose stuff. your vids teach me a lot.
@Vekoh2 жыл бұрын
Im from NZ had a few mates have similar issues with internally gated turbos, in the end the wastegate hole the flap closed on needed to be ported as the hole was ridiculously restrictive. Had it happen with an Rb25det series 2 and Rb25det neo. we also replaced dump as they're pretty restrictive too
@mohamedomarbelhajali33852 жыл бұрын
you can try to port the wastegate flow path in the exhaust housing so u have less pressure
@youtubeuseronalot63762 жыл бұрын
Loving this S14 fix & DE+T episodes makes me want to do a EJ204+T to my Impreza ....U'll figure it out Jimmy & give us top content doing it😎😎😎
@UsedLegacy92 жыл бұрын
I’m the same, been wanting to +T my ej251 for a while now and this is just feeding that want even more.
@youtubeuseronalot63762 жыл бұрын
@@UsedLegacy9 try 'home brew subaru' on KZbin he's done eg2.5+T stuff ages ago on his channel
@ReignitedAuto2 жыл бұрын
As frustrating as these sorts of problems are, they are the ones where you genuinely learn something new. You'll get it dialed, and it'll seem obvious in hindsight. 👏👏👏👍
@skylerterry85062 жыл бұрын
4:25 the way Donald rubbed the s14 🤣
@pontuslarssoonn2 жыл бұрын
As other comments are suggesting u might wanna check the wastegate flap inside the exhaust housing, so that the flap is actually opening as it should. The arm might be broken off of the flap or something, and the flap might be stuck.
@jacksongaulke40162 жыл бұрын
Had this problem on my E30. Port the gate. Helps a lot. I wasn't totally comfy with it through, so I went external for simplicity sake
@wyattmd0032 жыл бұрын
I have a 2860rs on my sr20det, I had to port my internal gate and install a bigger flap to get it to control the boost spiking
@empracingau2 жыл бұрын
I had a s14 sr20det in a 180 doing this with a 2871 and a disco potato the lowest boost I got was 18 and kept going up near 300hp no matter what I did including an external gate!! Put a stock 2560 on and it got sensible 🤷♂️
@jamesclev92 жыл бұрын
You have a spot in the middle of your lens coming through on the video, little purple dot, maybe from recording welding arc?
@twinstealth2 жыл бұрын
I just can't wait to see all of the s-chassis all running and together!
@kingp002 жыл бұрын
Look at the wastegate port in the turbine housing. It may need cleaning out even porting (especially if it's a Chinese housing)
@red_zed332 жыл бұрын
Check the actual flapper of the waste gate. You wouldn’t see it from the outside, but the lever may be “engaged” on the outside but it must closed or not fully open on the inside. Turbo seems fine. Vacuum source is fine. Timing is fine. Must be that mechanical issue. New manifold would likely fix it.
@WhiskeyGulf712 жыл бұрын
I would be inclined to run a stock DET clutch, that way you have a weak point that is not the rods ! Surely if there was a restriction in the exhaust that would impede the turbo as the gases are not flowing freely. My thinking is that the gate port is either obstructed or insufficient to allow the excess exhaust pressure through, gate wide open should essentially turn you engine back to N/A. Also check you have sufficient oil pressure to the turbo, if that’s just free spinning it might account for the over boosting & the bearings will have a lifespan of milk on a hot summers day.
@philip22nz2 жыл бұрын
You need to add back pressure if you want your current setup to work. Otherwise you need to port the wastegate but need to do that correctly or you'll have other issues also.
@andrewwhite93192 жыл бұрын
Had the same issue on my s13 rally car with a 11-1 compression SR with the same 2860 turbo. Had the internal gate machined out and a gt30 waste gate flap fitted. Pulled it from 13-14psi minimum back down to 8-9.
@andrewwhite93192 жыл бұрын
Also running a stock manifold.
@louiswun2 жыл бұрын
You need to port and enlarge the wastegate hole to smooth out the flow path
@jintyjohnsonable2 жыл бұрын
Same thing on my 3sgte. Wastegate port is way too small on these turbos. I had the same issue with 2860rs. Port it, it’ll help a ton
@JRCOZY2 жыл бұрын
Port internal wastegate hole, spray paint with flapper closed and port right out using paint as a guide.
@zackaryallyn27252 жыл бұрын
Had this problem as well. Was only able to fix it with external waste gate. Was on the ecotech 2.2l and not a sr but thats my 2 cents
@EXZACHTPERFORMANCE2 жыл бұрын
Perhaps the size or lack of, in the runners of the exhaust manifold, coupled with the higher compression, and potentially not enough flow through the flap of the gate in comparison to the efficiency of the turbo are just making boost too easily, changing one thing clearly wasn't working so maybe it wasnt just one thing that was causing it? Lot of the Barra guys over here in aus port the wastegate flap if staying internally gated because it quickly becomes difficult to control boost. Or like a lot of other people are suggesting maybe the flap itself isn't rotating with the shaft
@therealbennewman2 жыл бұрын
Had to port my internal gate in my turbo to stop boost creep, its usually to do with the manifold Design even thought the stock manifolds are fine up until about 350hp ish. bigger rear housing can help aswell
@aaronsigley20532 жыл бұрын
Smooth out the harsh edge of the wastegate port where the exhaust gas flows to exit through the flapper. The smoothing would be performed on the turbine side. Use a carbide burr bit. Usually helps with boost creep. Also SR’s suck.
@darxxtuff2 жыл бұрын
ANT BuzzKillington at 2:45! 🤣🤣🤣
@joellabrecque56962 жыл бұрын
Brian with the inspection glasses 👓🤣
@c54371082 жыл бұрын
Id check that downpipe off the turbo maybe the downpipe was intended for an external gate w a mad restriction to the internal waste gate dump at the back of the exhaust housing.
@TheEndDweller2 жыл бұрын
Connect the external boost gauge to ensure it matches the ecu map sensor
@Dirtyz12342 жыл бұрын
Really need to pull the downpipe and check the waste flapper function and make sure the path is free.
@theguru-s2l2 жыл бұрын
I agree with lots of the comments saying what i think too. Porting the waste gate out may help, id also make sure that the wastegate is functioning as it should on the inside. A larger turbo would spool slower, and decrease the low end torque but up the hp on the top end. For some reason i love a t04e.
@KristoffJohnson2 жыл бұрын
Easy fix there bud! Throw some bigger injectors at it to support some corn and ignore the creep. Problem solved. It'll live at 20psi....😎
@bigfich1232 жыл бұрын
made 280rwkw on stock manifold with a GTX2867r on 22psi. take the dump off see if the flap is fully openiing
@sandygarage38022 жыл бұрын
My DE+T on the dyno, was unhappy on 91 (pre-ignition?) Fuel was changed to 98 & it ran a lot better. Because of a boost creep issue caused by a small rear turbo housing, the boost is set at 8psi. The wastgate on my turbo is an adjustable Turbosmart IWG. I also have stock plugs,leads & distributor. The exhaust on my car consists of a tubular manifold, 2.5 inch stainless exhaust with 200cpi cat & Vibrant rear muffler.
@VLNath2 жыл бұрын
if the gate has been wired opened or whatever and its still making all the boost the only answer is the wastegate is to small.. strange just that tad more compression would make such a difference but it seems the only answer.. either port the gate hole or change the housing.. if all else fails its worth a try just to find out
@anthonylong46112 жыл бұрын
It could possibly be cam overlap. Not too familiar with SRs. I would also hook up another gauge to double check that the boost you’re reading is correct. I’ve had plenty of brand new sensors read incorrectly making me scratch my head for days.
@joemurray96692 жыл бұрын
higher compression could be causing you to get boost creep compared to lower compression. might need to do external or bigger downpipe and exhaust.
@bricebertelsman77832 жыл бұрын
You need more subs brother your channel is good as hell
@jasonpetrich41412 жыл бұрын
Yep time for a port and polish
@griplimit2 жыл бұрын
If you wanted to keep the power under 300 whp you should have put a T28 on it. I’ve had this exact issue before with a GT2871, the internal gate just don’t flow enough air to bypass the larger turbine housing and wheel. GT28 series turbo’s like to be between 15-22 psi.
@louiswun2 жыл бұрын
If any GT28 size turbo, if the compressor able to flow 400hp, if the exhaust housing is 0.64 AR, I port and enlarge each and every wastegate hole to make sure it won't over boost
@dogsvs57322 жыл бұрын
Wonder if an anti-surge housing for the turbo would help. The cold weather is also a factor more boost.
@TheKumaKuma2 жыл бұрын
Might be tike to get some connections in Australia. They may be able to give all the info you need.
@petersalas52152 жыл бұрын
dang Jimmy O repping Flipzco. Lets goooo
@shan3_o2 жыл бұрын
you'd almost assume that the flap has been wielded shut in the turbo for it to still be making that kind of jam, when i fitted a 2871 to my det i pinned the gate open to drive to get tuned and could barely get 2psi at like 6k rpm. i'd take the elbow off and look at the gate operation
@TheApexofthevortex2 жыл бұрын
I used to have a 5th subaru legacy GT that had the same issue, no matter what we did it would always overboost when I put a 3 inch downpipe on it. Not sure what kind of downpipe you're using but theres a good chance there isnt enough restriction in the exhaust and too much restriction in the wastegate itself. You either need to enlarge the wastegate port or run a an external gate, anything else would be a bandaid fix.
@base23852 жыл бұрын
The limiter finger bounce is the funniest shit man hahaha
@mmodtomic71192 жыл бұрын
@15:54 Hold on...freeing up the exhaust will just PROMOTE boost creep, right?
@michaelweber16942 жыл бұрын
Borescope the flapper make sure it moves and is not seized and the shaft is freeweheeling
@tristanbaker58602 жыл бұрын
I expect you’ll need to Port the waste gate port on the turbo, I expect the port is restrictive and causing the exhaust gasses to keep spinning around the turbine
@22rered292 жыл бұрын
the sr20de just wants to show the det's in the shop it can hang with the big boys
@The_Impulse2 жыл бұрын
I am using the same turbo on a built Honda D-series with 11:1 compression and having the same issue. (Tuned on the link Honda standalone) we think that the internal wastegate is too small to control the turbine speed and ended up adding a 38mm external wastegate. Getting tuned tomorrow so hopefully it works.
@semirm82482 жыл бұрын
Its a higher compression engine and internal gate has a small exhaust exit I had a similar problem on my subaru. Put a external gate and be done
@gateaccess8182 жыл бұрын
remove some of that preload off wastegate, more preload, more bost presure it takes to open the gate. the closer the gate is to a nutral preload the quicker itll open.
@s-chassis1232 жыл бұрын
Had the exact same issue with my Sr20 with standard turbo. As soon as I did front mount, full exhaust with dump and stared tuning it, it would just creep boost. It’s just due to the hole in the rear housing of the turbo being too small. Only real way to fix it is go external gate. Stock internal gate sr turbos suck for boost spike. I had a 14psi spring that worked perfectly but it would spike to 19psi and then level back out to 15
@s-chassis1232 жыл бұрын
Also the stock manifold’s are relatively restrictive so it doesn’t help trying to get all that exhaust gas out quickly and efficiently. Mine did get better when I put a stainless low mount manifold on it but still didn’t fix it
@mattches_132 жыл бұрын
Could waste-gate be blocked on the manifold end? 🤔🤔🤔🤔
@MrRoven0092 жыл бұрын
Wouldn’t matter they pinned it physically open
@taylor_drift2 жыл бұрын
@@MrRoven009 they pinned the arm open. It was mentioned in another comment that the physical flap could be seized and the arm broke off, basically doing nothing. Unlikely, but so is everything that has happened thus far.
@matthewhickling13502 жыл бұрын
Ty so much, those bangs gave me the hugest smile 😂
@Reddude1022 жыл бұрын
Check on the wastegate port going into the down pipe for some sort of restriction
@rowaldwousie52892 жыл бұрын
1 thing i learned watching jimmy , adam , tommy , rudnick. Is that dj always late😂😂😂😂
@danpaulus17062 жыл бұрын
Go external gate, had this issue with a obxt 2.5l turbo outback that would spike to 20-22 psi in cooler weather
@Nito973_bnb2 жыл бұрын
Not gonna lie I’ve been learning about turbo a lot better watching you guys thank you 🙏🏿
@adamwelcome7382 жыл бұрын
I've done this swap personally. Regardless of what engine turbo combo always achieve a linear boost curve.... imo waste gate flap damage and or the dump pipe is stopping the flap open correctly. The latter I have seen personally on s14 with a aftermarket dump pipe. Sr is good.
@ThatHoodlum192 жыл бұрын
Port that wastegate hole mate!! Also, you don't need to wire the flap open when testing the wastegate port. Just simply unhooking the actuator arm is enough. The gases will smash that flap open. My disco potato(GT28/60 RS) on my RB20det has a similar problem although mine is less effected. Spikes to 19psi but drops back down to 17ish, that's with a 14psi actuator. So if I port the wastegate it would be fine but that's around the boost I wanna run so I left it. Also 2 step will ruin that stock NA sr, just so you know.
@ThatHoodlum192 жыл бұрын
NA high comp probably pushing a lot of gases too.
@mario86202 жыл бұрын
Check vtc timing at that rpm, and also can be wastegate exhaust port is not big enough
@wobblysauce2 жыл бұрын
Compression is only a bad thing for weak tunas. Looking at the gate in its location with the one from the Black Z, the throw is not wide open. So have a look at the Flapper, you could do some porting to make it flow better.
@Apersonmrrw2 жыл бұрын
Get my man Ant a heated Milwaukee jacket, he's freezing !
@YOUKNOWUDEAD22 жыл бұрын
Ok hear me out!! A "where's Donny" merch drop.. with his face looking through a broken door.. just like the shining movie..
@crxpablos2 жыл бұрын
Do a pull with the wastgate open, actuator disconnected, bet it still makes a bit of boost