The spark plug wires bouncing up from pressure was inexplicably funny to me
@rmp5s Жыл бұрын
Same here. rofl
@jeffryblackmon4846 Жыл бұрын
I thought it was time to play Whack-a-Mole.
@D41Michigan Жыл бұрын
Coils, no spark plug wires on these. They are coil on plug.
@xxprouxx Жыл бұрын
@@D41Michigan right. My bad. Just the first thing that came to mind LoL.
@D41Michigan Жыл бұрын
@@xxprouxx lol your good 👍
@deansapp4635 Жыл бұрын
As a 34 year retired auto mechanic, shop foreman, etc, If i lived close to Eric, I don t about 700 miles away, I would love to volunteer to help him do these tear downs. I will be there one day cause visiting Eric s shop is on my bucket list. I never miss a video
@frankdesbaux Жыл бұрын
Yeah, me too. I'd sweep the floors and make great food and get the beers.
@OingBoing-bh5vm Жыл бұрын
Same A Live Show.... 😮 I'm all in !
@mitchhedberg4415 Жыл бұрын
Thanks, but that gets creepy when strangers want to show up and be pals
@Conservator. Жыл бұрын
@@mitchhedberg4415 We’re all car lovers, aren’t we?
@scenicdepictionsofchicagolife Жыл бұрын
@@Conservator.without a doubt
@stephanebolduc6501 Жыл бұрын
Very educational, shows what happens when an engine gets frequent oil changes, man was that engine was very clean! Thanks for sharing Eric!
@jamesplotkin4674 Жыл бұрын
And regular BK engine flushes would result in much cleaner rings and lands.
@harrywalker968 Жыл бұрын
yes,,but it was driven like a horse & cart,,not a fkn race engine, like it should of been, direct injection is the problem.. carbon.. de carbon that engine, last forever.. there basically bullitt proof if DRIVEN.
@kenthorkveen1 Жыл бұрын
I'm going to say it's the carboned up vales.. it probably was causing a misfire, as well as the staining you see from it possibly being lean.. great video as always!
@lustfulvengance Жыл бұрын
Yep you beat me to it! I guarantee you that's all that was wrong with this engine probably cylinder two and three weren't making good compression due to carbon and somebody just said the hell with it swap the whole engine instead of fixing it
@richs7362 Жыл бұрын
Yep I have one of these in a 22 Maverick. They are known to carbon up the seats of the valves, been told it's the number one problem. I installed two oil catch cans on the PVC system to help with this issue. I know when he looked in the ports it did not look good, should have removed the valves.
@MrTonyPiscatelle Жыл бұрын
@@richs7362 You also have to consider that its direct infection, and what kind of codes that will bring up while in a starting sequence. Couldn't be good .
@shadowopsairman1583 Жыл бұрын
Ford, circled the problem
@FoxFaderWorld Жыл бұрын
Mine were worse on my 2L EB and I had no misfires. It is possible though.
@dustcommander100 Жыл бұрын
That engine has the coveted "Whack-A-Mole" option! Seriously, I'm with you on that keyless crankshaft - I think they're saving a dollar by eliminating the keying operation - and gaining several dollars by selling those magic washers. That little pep talk at the end reminded me of a painful lesson I learned as young man : I bought a rim from my local salvage yard, and took it to a tire shop to have a tire mounted on it. The tire shop had the foresight to check the rim, instead of just putting the tire on and sending me on my way - and the rim was warped. So I took the rim back to the salvage yard and they gave me another. This time, I mounted the rim on my Jeep and checked it before going to the tire shop with it - and it was also warped! I went back to the salvage yard for another, and asked them if they had a way of checking them. The gentleman said "We sure do - we sell them to someone like you, and if they bring it back, we know it's bad". Ouch! So glad to know you don't do business like that - and I really enjoy the videos!
@mikehughesdesigns Жыл бұрын
Whew! Good to know I'm not the only one with the Whack-a-Mole thought...
@mark37f Жыл бұрын
I think Eric is wrong in his statement about yards caring about what they sell. The mantra in that biz seems to be "you pays yer munnys and it's yours".
@Conservator. Жыл бұрын
Great story, a little bit sad but it made me smile nonetheless. Tx!
@damienvillano4044 Жыл бұрын
It's called having integrity, or pride in your work. Sadly it is not the norm today. Find the good guys out there and stick with them! Also spread the word about them!
@Conservator. Жыл бұрын
@@damienvillano4044 💯
@heinrichgerhardt6119 Жыл бұрын
I rented a 2018 Focus ST in Germany and drove several Alpine passes with it, 2 laps on the Nurburgring, and cruised at 140+ mph on the Autobahn. Great car and great engine/trans combo. Even the Recaro seats were excellent (if you're under 200 lbs).
@filmboy18 Жыл бұрын
They are good cars but the engine does have its limits. They can't be pushed too much as the pistons and rods are only safe for around 300-310hp (at least for uk build focus st250). However, the block is pretty strong.
@chadmcquade3075 Жыл бұрын
I weigh 240 an the seats are fine for me mine was great for 5 years I gave it to my son for his 16th bday an bought a type r
@justsumguy2u Жыл бұрын
I think I see what was going on here. The yard sold the customer a perfectly good engine, but customer had driveability issues that they falsely attributed to engine mechanical problems, so they returned it. I'll bet the customer bought another engine after that, and had the same issues.
@d.b.1008 Жыл бұрын
May missdiagnosed..Turbo failure?
@pubbiehive Жыл бұрын
Maybe electronic issues?
@justsumguy2u Жыл бұрын
@keenanmolver9689 Maybe it was the turbo. Customers are quick to replace things instead of performing accurate troubleshooting techniques
@justinryker3264 Жыл бұрын
Seen it before, dude replaced an engine and had exact same issue. Catalytic converter was plugged lol
@ElectricSwordfish Жыл бұрын
He mentioned a tight spot when 2 and 3 were at the tops of their bores...maybe that was the issue? Mechanical binding can trick the car into throwing a misfire code
@BigAlsGarage Жыл бұрын
20 years as an OEM Ford tech here, and I enjoy all of your video's, and have even learned a few things off of a few of them! Spot on with the outro about the industry, I see so many mis-diagnosed things come in for repair with sometimes a few thousand dollars of parts store coils/PCM's/ect hung on them over what usually turns out to be a few hundred dollar fix, it's sometimes unbelievable. Proper diagnosis is the most critical part of any repair as you have stated, especially with the complexity of modern vehicles.
@brothertheo2677 Жыл бұрын
Gummed up valves caused low compression and/or leak down. That is why the plugs were out.
@davidroosa4561 Жыл бұрын
thats what I think
@markae0 Жыл бұрын
valves looked horrid
@AKAtheA Жыл бұрын
these do not have hydraulic lifters, the buckets come in several sizes and are matched for a fixed gap. This is fine for 50-60k miles, then it needs adjustment. To do so, the shop has to remove the head, measure the gap, order specific buckets, remove the camshafts, swap the buckets, put the head back together, check the gap (and prey they got it right...), bolt the engine back together. This costs over $1k to do, takes about 3 days (waiting on parts) during which the shop has a non-driveable car taking up space, so it's rarely done when it's supposed to and the valves and seats get beat to death from the excessive gap, causing compression loss. All because Ford was a cheap c*nt.
@tomscott1159 Жыл бұрын
@@AKAtheA Jaguar got away with this scheme for 40 years on the XK engine. But it was not meant to be a mass-market engine for the riff-raff who couldn't afford the shop charge and a back-up vehicle. In the design phase some boy wonder must have convinced somebody that through a miraculous new process, wear in the camshaft, bucket, valve, and seat would be eliminated. It is sad to see so many of the new engines, with so many wonderfully designed and built aspects, have one or two fatal flaws. This is the nature of piling-on so many innovations into one new product: all it takes is one mistake and all that good work goes for nothing. EV buyers should take note and tread cautiously.
@AKAtheA Жыл бұрын
@@tomscott1159 Honda (bikes) and Toyota (the legendary 2JZ) use this successfully for years, but in applications where it makes sense - like revving the engine to the moon and back. It's kinda' retarded on an econobox that redlines before 7k RPM, the customer literally gets no benefit here. Whatever was saved on a set of rocker arms and lifters (heck, ditch the lifters if you must, but give it adjustment screws) is eaten by the adjustment procedure...
@s0lidgoat199 Жыл бұрын
Wow 2 years since the last 2.0? Feels like 10 months ago. Time sure flies when you work hard! Keep it up.
@jeffryblackmon4846 Жыл бұрын
I in no way feel shorted if your teardown reveals an operable engine. It was an interesting video, Eric.
@reviewaccount469 Жыл бұрын
I could care less if the engine being torn down is bad or good. A good engine is better for Eric, so as long as I get to watch a teardown I'm happy.
@blakebritain9787 Жыл бұрын
Big turbo on my ST pushing 70k miles now 👍🏻 love this car so easy to work on!!
@fuse8052 Жыл бұрын
Mad respect Eric. I've worked at yards that sold engines that we were never able to test. You have integrity and standards. Please keep being you
@WhoThisGuy515 Жыл бұрын
The key thing is just them saving money by not machining the cranks and the pulleys for a key. I've been a machinist for many years and key ways usually have a .001 tolerance on the width and key and the location is also usually a plus or minus 1 degree tolerance. The current machining rate (my shop) is about $145 an hour so if they can save that for the millions of cranks they produce, that;s a huge amount saved.
@jimmyaber5920 Жыл бұрын
I worked for a car manufacturer as a trainer and field support. When theb keyways went away in the early 90s the info was that tolerance drift and market emissions adaptability were why gears quit being keyed. The cam setup and crank positioning was blueprinted like hotrodders have done for ages. If deck height or cylinder deck to cam centers varied then it was handled. If turbo and non-turbo engines had two ideal cam setups then the robots and the dealer service tools handled it.
@timbutton4990 Жыл бұрын
Your hitting the sweet spot.
@benthurber5363 Жыл бұрын
Isn't slotting one of the more expensive processes? Like, the joke I picked up is that the best way to make money with a slotting machine is to not buy one.
@lindsaydempsey5683 Жыл бұрын
I appreciate this video, even though the engine wasn't broken. I own a 2014 Focus ST, and this video was really helpful for me. The internals look far more stout than I was expecting, so I guess I can feel good about leaning on mine a little harder in future. I do wish that they had port injection to limit in the inlet valve fouling, aside from that I'm really pleased wit mine, it does everything advertised on the outside of the tin.
@Ar0d Жыл бұрын
Spray some Seafoam past the air filter and it'll help clean that stuff off
@lindsaydempsey5683 Жыл бұрын
@@Ar0d The ideal thing is to get it into port if possible. 69000 km on mine, no stutter yet, but it must be coming 🤔
@SeanPwnery Жыл бұрын
Will leak-downs make their way into teardown videos before they come apart after this experience? Might add a few minutes to each video, but it would definitely help explain the situation too.
@I_Do_Cars Жыл бұрын
I suppose it may on engines with no obvious problems
@chubbysumo2230 Жыл бұрын
@@I_Do_Cars the fact that 2 and 3 were not making enough compression to pop the coils out was concerning. wonder if the customer did a compression test and found that 2 and 3 were low. if the rods are compressed even just a bit, or even a bit bent, it would lead to poor running because of lower compression.
@I_know_what_im_talking_about Жыл бұрын
@@chubbysumo2230- yep. Could have idled just a tiny bit rough due to even the carbon build up on the valves and was declared as “not good enough” and pulled back out. 🤷🏻♂️
@keithwalton Жыл бұрын
@@I_Do_Cars As others have said, the coils not popping on some cylinders could be due to low compression, but could just be you didn't crank it at the same speed on those cylinders. Stuck rings looks to be the most likely cause. The engine otherwise looked barely bed in. Bearings initially look bad then improve in the first 100 hours.
@harrywalker968 Жыл бұрын
@@I_Do_Cars old bikes, 1930,s had cone clamping.& machines,, easier manufacturing, never had any probs with them. &, id say harleys still use it, cos there pre historic relics of bikes.. i have a focus, tdi. 2.0. goes like a cut cat..5 lt 100. 08..ausie..
@goaliepro1996 Жыл бұрын
2014 ST owner! Saw your last video about this engine, one of the most clean tear downs on the channel
@stephengreen3566 Жыл бұрын
I have a Duratech 2.0 in a 2005 Ford Focus and I have 138,000 miles on it. I have changed the valve cover and gasket, plugs, and coils. I noticed, when I was in there, that I will have to change the timing chain in the next 40-50,000 miles and it seems to be a pretty simple job. It uses the same "diamond" washer on the crank so you have to have a tool to keep the crank in the correct position and a bar on the head to keep the cams in place. Other than it being a tight fit, doing it in the car, it is really a simple job. I have no complaints with this engine. It is much better than the new "wet belt" system Ford is using now.
@metronorthrailfan2244 Жыл бұрын
Oh yeah an engine in that condition could most definitely be rebuilt. I was not expecting a teardown like this. What also made my day was the high pitched voice. Not making fun but the editing with that was great. Great job as always Eric.
@auntbarbara5576 Жыл бұрын
18:10 was waiting for u to tap the tops of the pistons w ur mallet like u usually do before proceding especially since u noted #2 and 3 seemed tight at the top of the stroke.
@andrecampbell691 Жыл бұрын
The engine looked well engineered and maintained.
@24roughing76 Жыл бұрын
I got up and poured a glass of Bourbon while i let a 2:00 ad for Pillow Cube play in its entirety. Showing love, friend!
@johnisabella5148 Жыл бұрын
Dude you're my favorite person who takes engine's apart just to find out why it's there, I'm sure other people do it but they are not as entertaining, I'll say I have a 2.3 version of that engine and I'm glad to hear all of it's shortcomings and why it's bad, I'm glad to know What to look for, you tearing down engine's shows us what to look for and how to fix it before it blows up
@shaunrathbun6649 Жыл бұрын
Listening to your last comments on this video is exactly why i like watching your channel..and i like Listening to you
@stevenslocum5031 Жыл бұрын
Great to see a 2.0 teardown. I'm hoping for a 2.0 Ecotec Turbo Chevrolet teardown. I always look forward to your Saturday night videos!
@dangsJ Жыл бұрын
Iv owed a Mazda 6i with the 2.3 auto for over 6yrs with roughly 185k. It’s a great work car. Zero driveline issues. Just bought a 13 ST with 70k. These two motor blocks being so similar gives me a lot of confidence. Thank you for the info.
@triathleteover5030 Жыл бұрын
This is same engine with my 2015 Ford Explorer ecoboost. With regular change oil and ATF. So far no issues and drives like a dream.
@marce289 Жыл бұрын
Channel is very informative and entertaining. You seem like one of those rare business owners who actually give a shit about its customers, very refreshing to see.
@kencreten7308 Жыл бұрын
It never sucks! Your videos are always good.
@rodneyhopper22 Жыл бұрын
Video is good product is the problem
@jonesallu Жыл бұрын
I very much like that this is a family friendly channel. I can refer kids to this channel without hesitation. Thanks for leaving the machismo behind. Your channel is great! Thank you very much - it takes a lot to make a good video, let alone a great one!
@mikefoehr235 Жыл бұрын
My expectations of Ford are very low and then to have a seemingly good engine torn apart was rather shocking. Nice to see someone actually did oil changes. The engine was super clean.
@verothacamaro Жыл бұрын
These are great little engines. Very reliable for the power output.
@newfie-dean5803 Жыл бұрын
Ford makes some of the most durable engines around…
@zacharyfillmore6424 Жыл бұрын
@@newfie-dean5803just if you neglect the transmission in the slightest bit. Or look at if funny. Sad things happen
@mattalexander541 Жыл бұрын
I love that you commented on the non keyed crank. My opinion…. Anyone who has worked on a fusion, or any other modern car without the use of a two post lift will often pull the crank pulley to make room to pull the engine away from the transmission and out the top. I would assume that that was done on this engine. So, the timing was enough off that the engine ran poorly, or not at all, but not far enough off that pistons dusted the valves. It happens on these engines. I would encourage any backyard mechanic to purchase a book or subscription to a reputable repair site before attacking a project of this scope. Unfortunately, if this is the case, the seller ended up taking the financial hit for a beginners’ mistake.
@Dogg1512 Жыл бұрын
Awesome video, very detailed, however what you referred to as the Cruise Control System (hose assembly) is actually the Vapor Canister Purge Valve Assembly, which when fail will push a P1450 Code
@douhacomcastnet Жыл бұрын
Eric, I think you forgot to check for disconnecting rods. I always look forward for that test.
@anthonybertone2336 Жыл бұрын
I was thinking the same thing,
@inothome Жыл бұрын
He did manually try to move the big end of the rods though. 18:00
@ZachSutton-rs7zo Жыл бұрын
I love your videos they are relaxing and informational keep em coming bud love all that you do
@fasteddie6585 Жыл бұрын
Stopped the video at 20:30 to post this and will finish it in a minute but I have to say that from what I've seen so far is that there was probably a fuel delivery problem causing the carbon build up around the ring lands which if true, it was probably smoking through the exhaust system making the vehicle owner think that the motor was bad. Unfortunate to see a good $3,000+ used motor go to waste but then again, you could freshen it up with new rings, bearings and polishing and maybe get $4k out of it. Outstanding videos BTW. Thank you! 😎
@felixcosty Жыл бұрын
Thanks for the video. WOW that van, really need a video about how it got that way.
@gregoryweber7408 Жыл бұрын
the industry you are in looks like fun, that eco boost motor looked ok, thanks for the vid sir
@Syncopia Жыл бұрын
Aside from the keyless crank, this seems like a well designed little engine that's easy to work on.
@two6520 Жыл бұрын
Dam! That van had a bad day, I hope no one was in it when the side was removed. Great video as usual, thanks for sharing with us!
@slickrick57355 ай бұрын
Have a 2013 Escape with the 2.0 and still running great after 150k miles. Oil changed every 5k full synthetic. Only issue now is an engine light for over boost. Trying to diagnose it at the moment.
@TheFalseProdigy Жыл бұрын
I had an fiesta st engine replaced after a blown head gasket, thankfully they did it for free under a recall. this video made me wonder what they did with my old engine because I’m guessing it was still in pretty good shape
@robbiek5oh7 ай бұрын
Engine looked great. Just short of 250k miles on mine. If you are having misfire and stalling issues at idle, check the fuel tank purge solenoid; they fail open and allow fuel vapors to be sucked into the engine at idle which is overwhelming. Not an issue under boost, but a big issue at idle. Dirty intake valves don't help. I have had two solenoids fail in 11 years so far on the same vehicle (ford parts, not aftermarket).
@WhittyPics Жыл бұрын
I used to work at a place that rebuilt parts and engines and I can tell you that we got a lot of returns of parts that tested good on the test stands. Maybe incompetence or maybe a little bit of fraud going on? We got a lot of good alternators back as defective. We also bought cores that were almost new and we loved those. Just about all the parts we good and reusable, though we put new brushes and bearings in everything.
@jaredreynolds6348 Жыл бұрын
Dangerously close to the 2.3 ecoboost from the s550 teardown I’ll keep beggin for it lol. Love the content bro
@177SCmaro Жыл бұрын
Valve timing with vvt engines is generally "close enough" as it floats around. So long as its in a safe range
@markfischer2472 Жыл бұрын
Been working on fords 10 years master tech. Replaced many 1.5 ecoboost for a design flaw in the engine block. Coolant would go into the cylinder(s). Most of the time it would set a check engine misfire code and the degas bottle will be low to empty. Replace a few 2.0 ecoboost but mainly the 1.5 had the most problems.
@caleb5962 Жыл бұрын
Your other 2.0 was what introduced me to your channel. I had just bought a fiesta st and my pops sent me the 2.0 teardown thinking it was what's in the fiesta. Still waiting for that 1.6l ecoboost teardown. I just got a big turbo for mine so if/when it blows up, I think I'd like to send it your way haha.
@samuelbeasonjr.3308 Жыл бұрын
Still absolutely loving your tear down videos and your often successful attempts to get those lost cause engines to run. Thank you.
@upsidedowndog1256 Жыл бұрын
You always provide good info on engines that have not much feedback.
@maciekapocaliptic Жыл бұрын
Hey, it's worth mentioning that from 2017 to 2019 a different block was used in fusion, escape and edge. 2.0 in the ST was always closed deck, while from 2017 in the models mentioned, Ford used open deck design and instead of improving cooling, they caused problems with head gasket failures (mostly between cyl 1 and 2) and mentioned cracking of the block.
@nafsucof Жыл бұрын
when guys do big power rs builds they use this block for the strength. mine is stroked to 2.3 and forged…
@Arrozconchopsticks Жыл бұрын
The 2015 Edge was the first to use the 2nd generation, open deck design.
@patrickdiehl6813 Жыл бұрын
Anticlimactic but equally entertaining. I second the motion for pre-tear down leak testing. It would also be neat to see the build and use a run test stand. Old school wasn't challenging before ecu but Im sure there's something semi universal that is out there, yeah I don't ask for much.....
@endospores Жыл бұрын
I like Eric holding the chain saying "Yes Yes" and you can almost hear the dollar signs
@jeffreydurham5342 Жыл бұрын
Wow, great way to check relative compression, take the plugs out, stick the coils back in and spin it see how high they jump! Great!
@wafflesnfalafel1 Жыл бұрын
Absolutely love that vid - sometimes engines are just perfectly fine. I was strongly looking to buy one of those Focus STs when they were new, great looking super fun car. But the ergo seemed set up for drivers significantly shorter than me, just couldn't get comfortable and ended up with a WRX instead.
@FoxFaderWorld Жыл бұрын
I'm 6'2 and bought one brand new in '13. Loved it, I had plenty of room.
@sethfirethornw101 Жыл бұрын
I think you might have my old motor. About a year ago I bought a 14 focus st. Next day started a straight up misfire on cylinder 1. I figured that it was just a dead plug/ignition coil but rather than trying to fix it I brought it back to the Ford dealership and they ended up just replacing the engine. The day I got the car I put fresh oil in it as well as a motorcraft oil filter. I know you said the date code was 2015 but I have to wonder if this was that engine. It's not unheard of for STs to get new motors after a previous owner blew the stock one up with either poor driving or bad tune.
@timteecvhn Жыл бұрын
Honestly, the engine pressure pushing the coils out and sucking them back in just after is inexplicably funny to me. Plus also the way you said "crack the cam caps loose" in this video made me just fukin lose it that's how hilarious it was haha. Gotta love the good ol' humor of missaying things intentionally in silly ways.
@bryanporter7545 Жыл бұрын
Say Eric… Anyone ever suggest attatching a piece of 5 or 7 ply plywood to the tops of the stand legs (with appropriate holes cut out) so that your drain pan sits above the legs and not between ‘em. Might make your job a lil easier and keep your floor a lil cleaner.
@johnelliott7375 Жыл бұрын
Good morning as always, thank you for sharing this with us as always Eric. I will have to look at the website to see if you have any of the stuff that I need. Great Sunday morning and enjoy your day today. Thank you for your time, help, and work.
@randellgribben9772 Жыл бұрын
i have a 2014 fusion with the vel 2.0 engine... 173000 miles on it.. change the oil with full syn every 6-7000 miles..put in 6 quarts and get back almost all of it. .minus a oz or two.. has a tune on it est power it about 280-285.. very quick and in cruise at 70 mph..i get 34/35 mpg.. here in the flat road os sacrament.. but can easily crest donner summit at 90 mph.. to go fly fishing.. the car and this engine is great.. never o issue from new
@randellgribben97723 ай бұрын
194000 ish miles now
@frankkent8046 Жыл бұрын
I would love to see a newer model 6.6 Duramax, or especially a LBZ engine! If I get some money, I will order a LBZ from you. Otherwise, I appreciate your video's, and you do a great job with them. I always look forward to seeing them each week! Thanks Eric!
@PieterBreda Жыл бұрын
Best looking engine on this channel so far. It seemed fine.
@Yoshimatsu414 Жыл бұрын
12:22 I think it’s the 2.3L Ecoboost like in the Focus RS and Mustang that’ll crack at the cylinder walls. They have thinner cylinder walls because they carved out bigger area for antifreeze to flow through to cool the engine better (open deck). Trade off is once you started adding more boost to those blocks or anything weird happens….crack.
@ifixthings86 Жыл бұрын
in 2017 (I think), they cut or drilled a passage between 1,2 and 3,4 for cooling, but it caused head gasket problems, overheating, and cracked blocks. This 2015 did not have that cut. If you go back and look, there is very little room to begin with.
@Yoshimatsu414 Жыл бұрын
@@ifixthings86 Damn I really hope not lol. I have a 17 Focus ST over a year ago now, I plan to start adding some power to it soon. When I bought it I did a lot of research and figured I would be safe with the ST's 2.0L. I hope they didn't build some 2.0 Ecoboost's with passages and some without in 2017. If that's the case, hopefully I get lucky or something lol.
@ALMX5DP Жыл бұрын
@@Yoshimatsu414if I recall correctly, ST’s do not have the issue as they used the same engine/head design throughout their production run. Other 2017+ Fords with the 2.0 Ecoboost got the “updated” head and gasket configuration.
@Yoshimatsu414 Жыл бұрын
@@ALMX5DP OK cool that's the conclusion I came to before I bought the ST. Was thinking about the RS but it was like $15K more and prone to the cracking blocks. I don't think it's worth the price different if I'd have to also change the block to start adding more power and not worry too much.
@RedTree-x9t Жыл бұрын
Eric I might be a bit new to this channel. I am from South Africa an my name is Jan. It is fun to watch and very interesting. It makes you feel that you can fix anything yourself, you make it look so easy. I most recently watch your video on the Volvo 70 R. What a SCORE! The reason I am writing you back on this video is once again, you show the carbon buildup in the intake port of a direct injection engine. Why does that happen? Most diesel engines are direct injection and why would the carbon bild up in the intake port so much? What causes it to do that and obviously you don't approve and neither do I. Fortunately I drive an ordinary single cab Isuzu pick up KB250 2016 with the Gen 6, 4J engine in it. It seems that I am lucky enough to have port injection as the injectors are to one side outside the valve cover on the intake manifold side. Best Pick up ever. No fuss, relaible and hard working. If you have done an explanation on one of your videos I missed, please send me the link below. Jan
@sfbfriend Жыл бұрын
Wack a Mole, that was funny. I have had several EcoPoop engines and except for the icky carbon issue on valves I love the power they put out and I personally have had zero issues. I am anal about maintenance. I also don't keep my cars much past 125K miles. Not keying the cranks is purely a cost saving move, broaching is expensive. My opinion. Thanks for another great vid, you da man.
@bradgreen987 Жыл бұрын
Another fun weekend teardown. Looked awful clean
@michaeltutty1540 Жыл бұрын
That was interesting. Doesn't really teach me much because the most "up to date" engine I have ever owned is the 400,000 mile Red Block 2.3 litre SOHC in my 1990 Volvo 240. Doesn't even leak or use oil to any noticeable degree. 4 litres in, 3.9 litres comes out. Since Arthur is a one family car the entire history is known. First car I have seen with 33 years and 400,000 miles on the steering rack, inner tie rod ends, antisway bar bushings, Panhard Rod bushings, and even one ball joint. Factory springs, although the front struts were done about 25 years ago. Rear shocks have been done 3 times. The car is eternal
@TheStiver Жыл бұрын
I don't know what it is, but there's something really therapeutic about sitting on your couch and watching somebody else turn wrenches after battling with it yourself all day.
@tally5k339 Жыл бұрын
Another great teardown, as always. There's just something fascinating about seeing how these engines come together, or sometimes violently fall apart
@kevincurry4735 Жыл бұрын
Good evening Eric. I have this engine in my Lincoln MKC 2016. That Van looks like the one someone Said Ray was in a wreck with early this week 😆
@OingBoing-bh5vm Жыл бұрын
" Don't worry, I'm a professional ." " Where is Blue & Hammer ? " " That was violent ! " I love ya man 😊
@pudermcgavin4462 Жыл бұрын
That is the cleanest I have ever seen of all the 2l I have worked on omg
@markujcich4245 Жыл бұрын
No worries, the mystery of this engine makes it entertaining. The range of comments on its engineering, possible failure, and return is a good read.
@Nadi-Ger Жыл бұрын
Reverse Whack-A-Mole, very nice! Oh, scared me with the Screwdriver in the chain of the oil-pump a bit.
@casob307 Жыл бұрын
Im gonna go with low compression, hence the difference in tightness of the head bolts which probably caused vibration issues. I notice a bit of skirt wear on a few of the pistons as you were examining them which would explain the minor wear in the crank journals. I would say who ever put this engine back together did a great job except they probably forgot or didn't do a great job of calibrating their torque wrench when tightening the head bolts. It's the minor details that make engine building so difficult to reproduce the same reliability of the oems. Probably ran amazing for the first 20 or 30k. Love the channel! It's greatly appreciated
@Mike-pr8hx Жыл бұрын
Love all your videos, there's always something new to learn. Is there a story about what happened to the contractor's van? It looks like Thor's can opener was taken to the right side.
@trose7620 Жыл бұрын
I think your motor there has major compression issues..Great vid!
@adey88splace Жыл бұрын
As demonstrated in the closing scene, with the proper amount of force; everything comes apart.
@Electro1016 Жыл бұрын
I have a 1.6 eco boost in my fiesta, I recently upgraded the turbo and about a month ago I started to get misfires at idle, they were pretty noticeable and car ran rough at times but never illuminated a CEL. After new plugs and coils and doing a misfire profile correction with no help I decided to clean the valves. The valves looked like the ones here. I manually cleaned them and the misfires were completely gone
@Simon__L Жыл бұрын
when you took out them 2 bolts from head that seemed loose... you think someone opened then closed them back or they were poor tight from factory ? gasket looked ok-ish but could have been a week spot on 2-3 ... specially when they bang same time ...
@jbrovage Жыл бұрын
this is the pre-open-deck design. the more desirable one. no head gasket leak issues, and a bit stronger. Glad to see it healthy, as i have a 2014 ST myself. planning on getting 200k miles or more out of it.
@thandomthembu4913 Жыл бұрын
Which year did they stop producing the pre-open deck design?
@Arrozconchopsticks Жыл бұрын
@@thandomthembu4913The first Ford to use the open deck was the 2015 Edge. Most other Ford's started using the 2nd generation, open deck engine from 2017 to 2019. After 2019, revisions were made to correct the coolant issue.
@mituc Жыл бұрын
In the Mazdaspeed community I've seen a lot of situations when people replaced all timing parts and even rebuilt engines because of accessories side poor maintenance, AC compressor pulleys and so on. It may be one of those cases with this engine as well.
@garyderian4350 Жыл бұрын
On keyless sprockets. Cam timing is set by the phasers and cam position sensors. As long as the cams are close enough, the phasers take it from there. Base cam settings are only used at startup when there is no oil pressure. On the engine, plugs were out, seems a compression or leakdown test was done. Maybe it was carbon holding a valve or two open.
@Jrv3192 Жыл бұрын
Keep up the great work Eric been away from the channel with family issues first video in a few weeks safe to say I've got a healthy back log off videos to catch up on. Keep up the good work sounds sad but your videos are one off the only things keeping me going at the moment
@I_Do_Cars Жыл бұрын
Keep your head up! Thanks for the comment buddy
@jrhalabamacustoms5673 Жыл бұрын
new version of whack a mole. Love your channel as always!
@CaptainSpadaro Жыл бұрын
12:30 The 'first gen' 2.0L EcoBoost was partially mentioned in the TSB Ford put out for coolant intrusion (15-16 Fusions and Escapes) when it was originally issued, but the TSB (19-2172) was revised ~2 weeks after initial issue to remove those applications. The Focus ST never got the 2nd gen engine (at least not for NADM production); why that is the case is unknown. The TSB doesn't say WHY the 2nd gen engines have coolant intrusion problems, but the general consensus is that the block and head castings have porosity issues.
@12345....... Жыл бұрын
You know your Fords
@CaptainSpadaro Жыл бұрын
@@12345....... it helps that I've got a 2015 Fusion with this engine, so I made a point of learning a few things about them (and buying a subscription to AlldataDIY). I will say that I have heard of coolant intrusion issues on 1st gen 2.0Ls, but there doesn't seem to be much, if any, rhyme or reason to it. A coworker of mine had a 2014 FoST (and the car was modded, though it was all bolt-ons IIRC) that started misfiring out of nowhere, and when he pulled the plugs, they were wet with coolant; he got rid of the car. One guy in the Fusion group I'm in on Facebook went through 2-3 engines on his car; conversely, another guy in the same group has over 200k on his and its the original engine; both cars are modded IIRC. Mine has been fine despite a minor overheat scare on Tail of the Dragon 2 years ago that I still haven't conclusively identified a cause for.
@airmotivewelding8012 Жыл бұрын
Would have liked to see the head, valves on the combustion side tell a tail. Color and pattern will indicate health. Another educational disassembly, thanks for doing these vids. I find it good for my Petrol Soul.
@terrynagle7410 Жыл бұрын
It's looks like a good one. My thoughts are it was put into an uninsured car that got recked. They pulled the engine out to return for some money back.
@proehm Жыл бұрын
Well, I have the non-turbo version of the same thing (even the same year) sitting out in the garage. So, I guess I am encouraged? The transmission is not all that we might hope for, but it has warranty out to something like 150,000 miles. I think I'll keep driving it the 3,000 miles a year that I do now until...
@SrgBlackburn Жыл бұрын
These engines tuned with no key can usual withstand up to 500whp before the timing can slip. Those friction washers put in some crazy work. It seems some auto manufacturers believe keyed cranks can lead to being a weak or stress point of failure for the crank there. That's what I've heard but not sure its true for the keyed crank.
@speed150mph Жыл бұрын
Honestly this goes back to what I’ve said before. I don’t know how much time you have to play around, but in this case if I were you, I’d pay the fee to get the block checked and honed, I’d get a ring, bearing, and gasket kit for it. Put it back together, and sell it as a reman long block.
@billrenfro9798 Жыл бұрын
Those engines had a problem with the block casting being to porous. Coolant would leak through the cylinder walls into the combustion chamber and be burned. The official Ford solution was to replace the engine. They had a recall to add a low coolant switch to the system to alert the driver of coolant loss. We had one in our 2017 escape. The problem showed up on ours with just over 30K miles. We kept a close eye on it since the engine ran fine otherwise and we would have to top off the coolant once or twice a year. We put just under 100K miles on it before trading it in. There were no external coolant leaks. Ford did replace some engines under warranty.
@nicholasvinen Жыл бұрын
I don't think that affected this generation of 2L engine, it was the 1.5/1.6L ones and the later 2Ls with the twin scroll turbo (from about 2016).
@yodasbff3395 Жыл бұрын
Another great teardown video, thanks for sharing 👍.
@andresquinonezramirez9373 Жыл бұрын
Hey Eric I own a 2014 Ford Focus SE/ST am been working on it to convert it to an ST about a year I swapped the factory 1.8L to the 2.0L for more pAwer (power) 😅😂 I did used the ford warranty to do this work but to be honest this engines are good for this generation
@christianmeeks4430 Жыл бұрын
Thanks for another great video Eric! Could we get a VW 2.0 CR TDI on the engine stand? Particularly engine code CJAA if you come across one.
@402SHO Жыл бұрын
There’s a 2.0 ecoboost in Omaha Nebraska U-pull it south lot right now. Last week I scoped the cylinders and pulled the plugs the engine is VERY CLEAN on the inside. And the engine is already out someone took the transmission.
@Sovek86 Жыл бұрын
I have a NA 2012 2.0, my valve train looked very similar to this. For some reason you do regular oil changes and those valve trains look almost new even after 90K miles.
@babaganoosh555 Жыл бұрын
I think the first clue was when the coils on cyl 2 and 3 didn't pop up like 1 and 4 did.... maybe valves not seating properly as others have stated...
@carnivorebear6582 Жыл бұрын
Exactly my thoughts after seeing that demonstration at the beginning (and then the lack of obvious damage otherwise later on to offer an alternative cause of loss of compression on 2+3) The only other option I see is incorrect clamping force on the head in those areas with the less tight head bolts (located around the area between 2 and 3), assuming the mating surfaces and gaskets were all in spec.