Something Isnt Right With My Mondeo ST..

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The Savage Garage

The Savage Garage

Күн бұрын

Hello everyone! Hope you're all doing well! Quick video for you lot to keep you entertained whilst youre all at home! Enjoy.
Business - savagegaragebusiness@gmail.com
Music - "Existence"
Instrumental by Temper Beats
KZbin - • [FREE] J Cole x Isaiah...
Spotify - spoti.fi/2SVDkjS

Пікірлер: 367
@ASH.......................1976
@ASH.......................1976 4 жыл бұрын
When you goes into that pipe it reminded me of mighty car mode where moog plays a radiator,intercooler like a harp !!!!😆
@lofty7180
@lofty7180 4 жыл бұрын
yerp, deffo an MCM moment
@ASH.......................1976
@ASH.......................1976 4 жыл бұрын
😀 !
@paulgriffiths6344
@paulgriffiths6344 4 жыл бұрын
I've played the drum brakes.
@ASH.......................1976
@ASH.......................1976 4 жыл бұрын
😆!!!👍
@ASH.......................1976
@ASH.......................1976 4 жыл бұрын
👍😆!
@CarlDavid1290
@CarlDavid1290 4 жыл бұрын
It's great to have you back James! Hope your safe and well in these current times. Congratulations on the 70k subs!! Many more to come
4 жыл бұрын
2 solution to the rought iddle : 1. the map sensor : to diagnose a bad map sensor : disconnect it and run the car : if the car run smother it's the map sensor. You may have broke it during swap. 2. The egr : it may be clogged up or malfunctioning and this is why the previous owner block the egr. Try to block the egr again (as original) and see if run rought. Good vidéo from France 🇨🇵
@nagymatyika
@nagymatyika 4 жыл бұрын
MAP is Manifold Absolute Pressure sensor, MAF is Mass Air Flow sensor.
@asherdavies3456
@asherdavies3456 4 жыл бұрын
There is a foam gasket that comes with the K&N kit, that is missing.
@jessktm4ever714
@jessktm4ever714 4 жыл бұрын
CONGRATULATIONS ON 70K you deserve it. I love watching your videos and seeing your posts on Instagram. Great man and I hope you and your family are healthy and safe.
@mikethompson7296
@mikethompson7296 4 жыл бұрын
Nice "Italian tune up" required. It'll blow all the crap out and pull the air out of the fuel lines. Great to see you working on it again, my favourite car of yours.
@TheSaabClinicUK
@TheSaabClinicUK 4 жыл бұрын
That air filter was filthy too. You need to wash it. Sit it in a bucket with some Persil washing powder and really hot water. Just half a cup of powder. Let that soak for 30mins. Then you need to rinse it through with a hose but from the clean side (inside) to the dirty side. So you push the dirt out. Leave to dry in the airing cupboard overnight. Ideally you should spray with K&N oil on the outside. Or a very light spray all over the outside with wd40.
@skodakatie7341
@skodakatie7341 4 жыл бұрын
Your video certainly eased the home isolation anxiety, stay well and safe James, looking forward to your next video!!.
@DazC2
@DazC2 4 жыл бұрын
The TDCI re-learns each cylinder over a 15 minute period. You’ve changed the dynamics of the combustion process by adding the EGR back to the engine that the ECU has adapted to live without. You’ll need to run the engine for an hour to allow all 4 cylinders to be re-adapted then it should return to normal.
@darren95mcinnes
@darren95mcinnes 4 жыл бұрын
Could be the previous owner had the egr mapped out when they did the egr delete so now you have put an egr back on it the ECU doesn't recognise it causing it to run rough. Congrats on 70k and its great to have you back uploading!
@georgemiller4585
@georgemiller4585 4 жыл бұрын
Darren Mcinnes it wouldn’t throw up EGR codes if egr has been mapped out
@darren95mcinnes
@darren95mcinnes 4 жыл бұрын
@@georgemiller4585 fair enough I never thought about 🤔
@chrissyscott1033
@chrissyscott1033 4 жыл бұрын
Finally someone with common sense George👍🏻
@snoopydogg1
@snoopydogg1 4 жыл бұрын
You can not map the egr out on a euro 4 tdci anyhow
@gavdaman21
@gavdaman21 4 жыл бұрын
On the electronic Egr they can't be mapped out, at least not when I wanted to do mine they couldn't.
@owenthomas3
@owenthomas3 4 жыл бұрын
I’m a apprentice in a back street garage and this pipe was my first job on my own and I dropped the only me 8m bold down the bell housing so had to fish that out with a magnet took me 35 mins😂
@hughjarse4627
@hughjarse4627 4 жыл бұрын
Should of used fallopian tubing rather than standard otherwise will crack
@robthesamplist
@robthesamplist 4 жыл бұрын
@@hughjarse4627 Not much Fallopian tubing about now though with this virus going around.
@AdammP
@AdammP 4 жыл бұрын
Two possible reasons which I can see, If the egr valve is stuck open it will allow unmetered air in.. causing this. Usually not a problem if they're stuck closed. Or air lock in the injector pipes , guessing you removed them to fit the seals.. they're usually self bleeding but you could crack them a bit of a turn at the injector and see if fuel comes out when it's running. Be careful though with high pressure fuel and use a rag if you do do it!
@ThermoNuclearLlama
@ThermoNuclearLlama 4 жыл бұрын
When you changed the injector seals you removed the fuel lines. Is all the air bled from the lines? Diesel is prone not to start well after being removed from the fuel. Might just need priming. Thanks for the upload :)
@arnoldkul3827
@arnoldkul3827 4 жыл бұрын
You don't need to prime the injectors in a common rail Diesel, only the filter if you have changed it
@shifty2755
@shifty2755 4 жыл бұрын
Modern diesels have a self purging valve on the fuel pump.
@nagymatyika
@nagymatyika 4 жыл бұрын
@@arnoldkul3827 Actually you have to. At first start the proper solution is revving the engine. These engines are famous for air inlet in the fuel system. :)
@ThermoNuclearLlama
@ThermoNuclearLlama 4 жыл бұрын
@@arnoldkul3827 thank you I didn't know that. I thought it was any air in the system needed to be bled.
@arnoldkul3827
@arnoldkul3827 4 жыл бұрын
@@nagymatyika That's not what I meant, what you said might be useful, I meant like you bleed the old tipe of Diesel engines with the Bosch injection pump, to unscrew the injector bolts and bleed the engine until only Diesel comes out and not air. The modern Common Rail engines are self bleeding. That means once the engine starts it should bleed itself out pretty quickly and the engine will run normal again, I'm not sure if it's anything specific to these Ford CRDI engines but I'm suspecting that the EGR is not working correctly and that's why the car is running like crap as he gets all those fault codes for the EGR or some bad vacuum hoses that can cause an air leak. But could be anything really with those modern Diesel engines. A proper scan tool for diagnosing is your friend in such a case.
@retrorestore
@retrorestore 4 жыл бұрын
I'd say there's a mounting plate or gasket missing from the MAF mounting for the K&N
@dillingerdan
@dillingerdan 4 жыл бұрын
Definitely is according to K&N themselves www.knfilters.co.uk/57-0577-performance-air-intake-system
@markellis4229
@markellis4229 4 жыл бұрын
Retro restores I think it’ might be air in the fuel system when he taken the injectors out . In the last video
@arnoldkul3827
@arnoldkul3827 4 жыл бұрын
@@markellis4229 It will bleed itself, these CRDI engines are designed this way.
@markellis4229
@markellis4229 4 жыл бұрын
The filter could need changing because the car has been sat for a while and Diesel causes bacteria in the filter which causes it to block and causes it to run like crap because blocked filters Will lead to a Fuel supply issue Starving The pump
@louisjames1062
@louisjames1062 4 жыл бұрын
retrorestore mr Martin a savage garage fan 👌
@stevebobojones
@stevebobojones 4 жыл бұрын
Hi Mr Savage has'nt your dad got the same engine and he had trouble with EGR valve ,check your MAF sensor,and Cars don't like sitting a prob at this time,when this is all over a lot of people will have trouble with their cars ,congrats on the SUBS you 've earned it ..
@Nathen9112
@Nathen9112 4 жыл бұрын
Sounds like the drive belt is on its way mate and crank pulley 😊. Just unslacken the union if there's any air in the fuel the ones on top of the injectors 1 at a time then tighten back up.
@1986timmis
@1986timmis 4 жыл бұрын
Give it a blast mate it's got air in the system
@CrazyPetez
@CrazyPetez 4 жыл бұрын
It's good to see another of your videos, James. I know K&N filters have a good reputation, but they aren't the best filter media, and if oiled too heavily, the oil can be drawn onto the MAF, causing problems.
@keithknight1107
@keithknight1107 4 жыл бұрын
Hi James good to see you back on if you want my advice I would do a bleed back on each injector to make sure you haven't got a stuck injector normally if there's air in the system Mondeo don't run and you're still does look forward to seeing your next video thanks
@PauloJRSantos
@PauloJRSantos 4 жыл бұрын
i agree with the idea of the map sensor, it can explain a lot things,even the smoke on the tail pipe! but im thinking you have a maxicom diagnose machine, its easy for you the check up for incoherences on the live data. greatings , keep on the good work
@malcolmyoung7866
@malcolmyoung7866 4 жыл бұрын
Hello James. The misfire is more than likely down to the work you carried out on the injectors. Air in the system(maybe) a poorly connected injector or break in the harness(wiring issue) etc. Although it’s a bit of work best put it back to ‘pre EGR/new ‘Carlos Fandango’ K and N and see if the car runs as it did before. If it does then it’s what you have added since the injector seals. If not then it’s more than likely to do with the work you did to the injectors. You need a baseline to work from. Poor running of diesels is down to a couple of basic factors ‘timing and compression’ usually. Inspect the engine around the injectors when idling. If there is any leaks around the injectors then the seals are either installed wrong or you may have forgotten to re secure the injectors in their seats properly. A poorly fitted injector will cause compression issues and poor running in a cycle set/misfire as will a working issue(not connected/poor connection/broken wire/open circuit) Also check that the injectors are connected to the harness correctly(unlikely as the harness only reaches specific cylinders) incase the firing sequence doesn’t match the engine timing. Great ‘vidjeo’ always enjoy watching..
@alferret1969
@alferret1969 4 жыл бұрын
The ECU needs to re-learn after fitting EGR. Best way is to remove battery for an hour, re connect, drive normally through all gears and varying speeds.
@brandonharding3115
@brandonharding3115 4 жыл бұрын
Al Ferret it’s been mapped out probably.
@colwyn9
@colwyn9 4 жыл бұрын
Dont put a cone on a diesel, it will sound like an air compressor. I put one on a 2.4L toyota hilux and it sounded naff
@Stu88Turner
@Stu88Turner 4 жыл бұрын
Yours is a euro 4 mate , difference between 3 and 4 is vacuum and electronic actuators, egr delete would of most likely been mapped out on a remap when the delete kit was fitted , also usually with the euro 4 you’d see a 8mm hole drilled in the cooler blank plate allowing your eml not to be on .... hope it helps you solve your issue
@Bucharestguidedtours
@Bucharestguidedtours 4 жыл бұрын
Great to see the Savage Garage back, best wishes.
@S-P-A-
@S-P-A- 4 жыл бұрын
Thanks for your vids bud. It is a funny old time at the minute but I've managed to fill some time enjoying your vids. Keep it up fella 🤘
@NikEastwood161
@NikEastwood161 4 жыл бұрын
I am fairly new to diesels and i recently changed injector seals on a 1.3multijet, it does sound like air in your system, bleed it out by whatever method is right for that engine and i reckon it will be spot on afterwards.
@chrisyoung5573
@chrisyoung5573 4 жыл бұрын
Love your video's James, hope you regain your enthusiasm for making them. Hope you and your family stay safe and come out the other end of the tragedy unscathed
@TheZXGuy
@TheZXGuy 4 жыл бұрын
Long time watcher first time commenting. Your videos are all great James and I can't wait to find out what's happening with the fiesta also hopefully you keep the enthusiasm and stay safe. You've given me the inspiration to start my own channel plus it gives me something to do through these quarantine times.
@nagymatyika
@nagymatyika 4 жыл бұрын
Check the real time data of mass air flow. On idle speed with opened EGR it should be around ~7g/s and with closed egr around ~10-12g/s. By the MAF change you can easily determine that whether the EGR is offed or not. EGR problem can cause misfire on a diesel engine and on this actual one air in fuel system also could. Try to rev up the engine several times and also keep it high rpm for a few minute.
@adammcallister2260
@adammcallister2260 4 жыл бұрын
Deffo air in fuel. Needs a good rev up to 2500rpm for 2 minutes. You can rule out MAF issues by just unplugging it :)
@keepingbritishcars4309
@keepingbritishcars4309 4 жыл бұрын
Your missing a foam gasket that should of been on the original that you move over to the k&n MAF sensor pipe
@simonhewkin8418
@simonhewkin8418 4 жыл бұрын
About to say the same 🤣
@michaelslater5669
@michaelslater5669 4 жыл бұрын
Good to have you uploading again bro! Love the yum cars merch 👌🏼 looks insane 🔥 keep up the vids to keep us all sane during this lockdown!
@NorfolkRoverworx
@NorfolkRoverworx 4 жыл бұрын
Hi James, hope you are well. I've had it in the past where when you disconnect the injectors and the battery is low, the pcm looses the injector trim codes. You should be able to re-input these with the Autel. It definitely sounds like a missing injector, so if it haven't sorted after a good run then check electrical connections on the injectors and check trim codes.
@clarelouise7040
@clarelouise7040 4 жыл бұрын
Hey unplug the electrical connector on the edge I guarantee it runs better I’ve had a LOT of Mondeo’s run in to this problem a few times and was successful in doing what I’ve just told you hope you and family are doing well
@mwmm
@mwmm 4 жыл бұрын
If I can suggest one thing, get an inline fuel filter in the engine bay (the ones with transparent sides) The fuel pump on these is notorious for chewing its own casing eventually and sending metal shards through your engine, it will ruin all your lines and injectors requiring a £3,000+ rebuild. Having an inline filter can help you spot this early, bad idle is also a telltale sign. Source; personal experience with this exact model and engine, also have a quick Google too!
@julianthomson7398
@julianthomson7398 4 жыл бұрын
You mentioned that the engine was smoking more than it was with rough running and smoking, check the egr valve is closing all the way. You should be able to use your scan tool to open and close the valve while the engine is running to check and on live data see the amount it is open closed etc.
@MrMarkeboy1234
@MrMarkeboy1234 4 жыл бұрын
That plastic looking mesh is called megamide. I use to use it when I made car vehicle harness back in my 20s.
@gavdaman21
@gavdaman21 4 жыл бұрын
I know exactly what that is. The Egr valve itself is stuck open slightly. I had this exact issue. Changed it and it was spot on. Didn't even try to clean it because apparently these don't like being cleaned.
@arthurgissing7387
@arthurgissing7387 4 жыл бұрын
they could be air in fuel lines from the injector job, need to run longer to bleed system. and mass air flow sensor is now getting more air flow essentially so needs a good run out so the computer (ecu) can auto adjust the mapping to make it run smooth. egr will kick in once engine is at optimum temp hopefully
@farley1992
@farley1992 4 жыл бұрын
Foam panel filters are better in these cars pipercross do a really good one , cones just suck in hot air from the engine bay, where as original box is a perfect cold air intake as standard
@harrypalmer7318
@harrypalmer7318 4 жыл бұрын
@The Savage Garage id say it could be boost pressure sensor too mine sounded like that was running really rough and no boost. Put that sensor on it drives brand new 👍🏼
@dmc4708
@dmc4708 4 жыл бұрын
If you’re worried about emissions, put a bottle of Forte Advanced Diesel Treatment into the tank before you go for the test. It’s good stuff, has been known to turn many failures into a pass.
@Noahmaelkekoo
@Noahmaelkekoo 4 жыл бұрын
Hey from Denmark! I've got a mondeo with the same engine as yours. It has got a faulty egr (stuck open) no loss of performance, no excessive smoke, no error codes only weird idle like you have well it sounds like it I had a mechanic mate check this for me and he confirmed this. I haven't changed it yet as the problem is only at idle, but I will change it soon and see if it fixed anything ;)
@superdiy7081
@superdiy7081 4 жыл бұрын
I had same issue on a Ford Focus 2.0 TDCI, turned out to be bad injector dumpping too much fuel causing smoke and misfire. Need do a injector leak test to find out which one is bad then replace it. Good luck!
@risingphoenix1187
@risingphoenix1187 4 жыл бұрын
Well I must say that this has been a good series so far. Don't pay attention to any of the negative comments, you are entertaining a lot of people and we truly appreciate your work. I recently went back to your first videos and now I am hooked to car mechanic simulator 2018. 🤣 Stay safe and stay strong in mind body and soul and I will pray for you bro. Keep up the good work. 👍🏾
@nikolil1031
@nikolil1031 4 жыл бұрын
Greetings and salutations from across the pond! We've missed you out here in Texas! Glad to see your doing well and still uploading. Stay safe out there. Your problem might be the maf is out of sync with your iac since you changed that air box and put on the egr. Just a wild guess though. Keep uploading as often as u can! 👍🇺🇸🇬🇧
@turbophl7259
@turbophl7259 Жыл бұрын
Throwback! Keeping The Savage Garage alive! We love in hope for some fresh uploads 🙌🙌
@pauldoherty8432
@pauldoherty8432 4 жыл бұрын
You need to get the system in closed loop , give it a good drive for an hour mixed driving.. the ecu doesn’t know if it’s coming or going atm .. great vids as always
@dannystirrups7691
@dannystirrups7691 3 жыл бұрын
40 quid for the k&n. Good deal compared to new. I got mine for £28 second hand when the weren't as popular.
@VSTV1993
@VSTV1993 4 жыл бұрын
Warm it up, keep on the throttle about 5% after its warm and idle then when you get a chance 3rd gear above 3.5k for 10 ish minutes. Even if its because of you had the fuel lines off. Your cooler might be blocked and your getting loads of back pressure
@Mike_5
@Mike_5 4 жыл бұрын
ST220 is a proper performance machine and with an air intake kit even more fun
@piotrekxbox360
@piotrekxbox360 4 жыл бұрын
Hi, check the injection system. The cost of repair is large. And it's not worth packing money if it breaks down soon.
@paul230373
@paul230373 4 жыл бұрын
That was a much needed video a break from all the bad news that’s going on great job 👍🏼👍🏼🤩
@xXJohnny1254eXx
@xXJohnny1254eXx 4 жыл бұрын
I've got a 07 reg Mondeo st that I've had for 2 years now, and its been plagued with egr problems. The egr units themselves fail about 8-12 months, u can make them last longer if u clean them, but cheap ones generally die fast, I've had 3 changed. The egr cooler is also problematic, prone to leaking, and leaking coolant down the egr system and intake, giving the same symptoms as a blown head gasket, normally blowing white smoke, then underload rolling coal. If its idling and stalling when accelerating, its most likely got a leak somewhere in the egr system, where the egr valve opens underload, but because its leaking and loosing pressure, it can disturb the pressure and blow back, acting like its got no boost and often stalling when trying to boost up. The fuel system bleeds itself after a few turns, the Delphi high pressure pump pretty much bleeds itself through fast, as I've replaced the mechanical pump unit and all my injectors myself, so that aint the problem. P.s, I've searched through the amount of crap on talk ford and other sites to try and find answers cos my ST just isn't reliable, and most of the people on their don't know jack xD my personal opinion is to do what I did and blank it off from the exhaust manifold, and put the bypass back on, then do a stage 1 remap to get some extra boost and also remove the engine light for the egr codes. I've done that 2 months ago and now I don't have to worry about it again.
@davidjnr3418
@davidjnr3418 4 жыл бұрын
I've had this before and it will be the EGR valve motor not adjusting correctly. Used ones are normally broken same on the Renault 1.9DCI engines they are well known for it. That's why it's smoking its the unburnt diesel etc.
@RevLexus
@RevLexus 4 жыл бұрын
Hello from Scotland, new to your channel! Great videos man!! The interior of this reminds me of the Puma a little :D
@buzzysteez
@buzzysteez 4 жыл бұрын
I think it's the gap in the airflow sensor and the air in the diesel lines.
@v4-goose147
@v4-goose147 4 жыл бұрын
Air in the fuel lines from when you changed the injector oil seals
@haydenfill8084
@haydenfill8084 4 жыл бұрын
Looks to have had a replacement gearbox aswell also the egr will be mapped out so you need to get it mapped again to re commission it
@d4ve587
@d4ve587 4 жыл бұрын
Can you do that trumpet trick again funniest thing I've seen KZbin lately 🤣👌
@simonevans792
@simonevans792 4 жыл бұрын
I have the same car but with a egr delete and passed an mot just need to give it a good run beforehand passed with flying colours
@darrenbrown-alternativerou359
@darrenbrown-alternativerou359 4 жыл бұрын
My diesel Astra had issues similar to this, I was told to run the car in 3rd gear at 50-70 mph for 15 minutes. Worked perfectly afterwards.
@stuartdavison8459
@stuartdavison8459 4 жыл бұрын
Glad to see you back great video looking forward to the next 1 during these weird times stay safe 👍🍺🍺
@fangface666
@fangface666 4 жыл бұрын
Tiger grip gloves 👍 much better than the black nitrile ones, last a lot longer! Excellent video fellow Norfolkite 😉
@TomRoberts2017
@TomRoberts2017 4 жыл бұрын
I'm sure that's a Jag EGR.. The mondeo one should have a vac hose and a breather... This might be your case as when my breather/vac hose blocked up it ran like a sack of nails
@kallumsteward9444
@kallumsteward9444 4 жыл бұрын
Also that air filter is of the v6 not a diesel
@225M3RCR
@225M3RCR 3 жыл бұрын
Not ture at all
@surviveasl
@surviveasl 4 жыл бұрын
when you delete the egr it is also turned of in the computer, you need to turn it on by software when you instal the egr valve back on
@heartattack7230
@heartattack7230 4 жыл бұрын
I love your mechanical videos
@-Dash-
@-Dash- 4 жыл бұрын
Starting problems and smoke from exhaust? If the EGR valve you fitted was not new(?) the 1st thing I would try would be to blank off the EGR again (and did you fit the rubber gasket on the top of the valve?). Use a piece of tin cut from an old beer/coke can in the shape of the metal gaskets you fitted but without the hole in the middle... Slide out the gasket and slide the blank in its place and retest. If that cures it then the EGR valve is prob no good.
@rorywrenn2577
@rorywrenn2577 4 жыл бұрын
If the previous owner removed the EGR, I would imagine it has to be mapped out so the computer thinks everything is as it was. Especially if when you bought it, there were no codes at all.
@classicgamer4451
@classicgamer4451 4 жыл бұрын
@Savage garage Hi James nice to see you back hope you are ok on lock down 👍
@brummiescot
@brummiescot 4 жыл бұрын
You should be able to test operate the egr valve using your autel as it has bidirectional control
@ashnyc90
@ashnyc90 4 жыл бұрын
Sounds like air in the fuel lines that explains it not starting straight away. On my diesel I need to crack off the fuel pipe unions one by one and turn it over till fuel comes out to let the air bleed.
@norm4242
@norm4242 4 жыл бұрын
Is that wise to do with the high pressure fuel lines?
@matthewthomson3828
@matthewthomson3828 4 жыл бұрын
I had same problem with mine. It ended up being a problem with ecu and to get it fixed was about £300. Aswell as the £60 check on ecu hope it gets sorted
@Beanie-4399
@Beanie-4399 4 жыл бұрын
When changing an injector on my 2.0 tdci ford focus mk2, it knocked and banged for a good 5 minutes until air was all out.. So to me it sounds like it's got air in the fuel system might be worth bleeding and trying.. if that doesnt help try taking egr pipe off and blanking it again as if guy has had it mapped out car will also go funny..
@MyJarrus
@MyJarrus 4 жыл бұрын
Blank the EGR again as the car is stage 1 remapped and in the map it probably says EGR off thats why running bad
@chrissyscott1033
@chrissyscott1033 4 жыл бұрын
Jarrus Killa he wouldn’t get an eml light on like he said if it was mapped out
@symonwallace1956
@symonwallace1956 4 жыл бұрын
There was no small hole in the blank plate that can cause the eml light to come on its common in vag cars to have small hole as it lets the carbon out but only a small amount
@lulzyboy
@lulzyboy 4 жыл бұрын
@@symonwallace1956 ford isn't VAG tho. also, the hole is only required for some 1.9 engines, not all.
@kallumsteward9444
@kallumsteward9444 4 жыл бұрын
Cant delete the egr in the map on these
@68xperfectx
@68xperfectx 4 жыл бұрын
Is it a after marker egr? I had problems with my saab replaced the egr with a cheap on and it just made the problems worse so gave the original OEM a good clean, no more problem that was 60k mile ago. Great video keep them coming
@ZintomV1
@ZintomV1 4 жыл бұрын
I reckon the EGR has been mapped out when it was blanked off.
@seanb9814
@seanb9814 4 жыл бұрын
Good video, but I hope you cleaned all the metal filings out of the intake pipe and filter before you started it? Keep safe.
@norm4242
@norm4242 4 жыл бұрын
It was a plastic tube, did you not see that?
@seanb9814
@seanb9814 4 жыл бұрын
@@norm4242 Nope, looked like a cast alloy pipe but now looked again. Still not great to leave those filings in there. Takes nothing to clear them out.
@brandonharding3115
@brandonharding3115 4 жыл бұрын
Could I ask why you put the EGR back on? They tend to be removed to save the engine on the life span.
@casperkezmorris8399
@casperkezmorris8399 4 жыл бұрын
Re fit the egr blanking plates see if it improves bet that second hand egr valve is nackerd
@dylanjoy4413
@dylanjoy4413 4 жыл бұрын
I think the old owner must have got it remapped or had the egr coded out of the system so the engine won't like being run with the egr, I got my lexus is220d remapped and it would do the same but just blank it off because it gives it a lot more acceleration
@evonation630
@evonation630 4 жыл бұрын
The oil on the k a n filter will get on your mass airflow sensor and brake it stick with stock Airbox
@Ricky12389
@Ricky12389 4 жыл бұрын
Do a full egr delete and get it mapped out also get rid of the open air filter as they just suck warm air in
@AnthonyHitmanFiore
@AnthonyHitmanFiore 4 жыл бұрын
Needs a good run out to rid the air build-up from when you did the injector seals.
@Stevewright442
@Stevewright442 4 жыл бұрын
Arty out an injector leak off test, sounds to me like a bad injector, also check the connectors at the injectors
@harryrobinson387
@harryrobinson387 4 жыл бұрын
Should of kept the egr deleted as it will create more issues later on just keeping blanked and get it remapped to get rid of the engine management light
@taximan7551
@taximan7551 4 жыл бұрын
Hope all gets sorted 🤞
@tylerraines3451
@tylerraines3451 4 жыл бұрын
Has your car been remapped with a egr delete ? That will be your issue if so
@syjames824
@syjames824 4 жыл бұрын
Did you clean the filings out before fitting the K&N? I do think there is air in the system and you probably should have primed it before starting it. A good blast is the best thing for it now though.
@AlanRafferty
@AlanRafferty 4 жыл бұрын
The only blanking plate my car had was at the EGR at the top of the engine, nothing had been altered at the lower point of the engine. The blanking plate you removed at the bottom looked far too thick to be a DIY effort by the previous owner. I think you should refit the lower one. Its an exhaust recirculation valve, by removing the bottom plate you may well have stopped it from recirculating...
@Itrique
@Itrique 4 жыл бұрын
I don't think you have to take off the bolt of the engine mount for the K&N bracket, you can also just put a nut on top of it :D
@chuckyfinster3686
@chuckyfinster3686 4 жыл бұрын
Did you prime the fuel system before you started it after the injector seals? Cant remember if you started it after you done them.
@chrismcgowan5180
@chrismcgowan5180 4 жыл бұрын
I know quite a few people myself icluded who would play a pretty penny for those gloves right now, haha
@3530lee
@3530lee 4 жыл бұрын
You have had the injectors out to change the seals. There will be a bit of air in the system, you will need to bleed the injectors.
@ASH.......................1976
@ASH.......................1976 4 жыл бұрын
It is crazy times I know ,I think the only thing wrong with the Mondeo is ,it needs some love 😊
@robwebster7406
@robwebster7406 4 жыл бұрын
Thanks for the vid 👍 and try getting some EGR cleaner 😏 I use it 3 times a year on my 1.0T ecoboost 👍
@tops3y
@tops3y 4 жыл бұрын
Good to see you back James. Stay safe
@dagenhamdave2611
@dagenhamdave2611 4 жыл бұрын
Hi james great vid Did u disturb the electrical connections to the injectors. Cant be air it would of cleared itself or unions nit tight enough and pulling air in??
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